Sheila, TVo
We noticed that the boost filter would cause the IMC to oscillate so we checked the OLTF again and found the UGF at 4 kHz, so we added +15 db to the servo gain and found a new UGF of about 30 kHz. This is probably due to the new EOM changing the modulation depth.
This seems high. The modulation depth is estimated to be only 3 times lower.
Yeah it did seem odd, but we reduced the gain by 4db here previously. So in the end it's about +11db which is close to what we'd expect from the EOM swap, maybe.