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Reports until 21:24, Wednesday 28 January 2026
H1 AOS
keita.kawabe@LIGO.ORG - posted 21:24, Wednesday 28 January 2026 - last comment - 11:55, Thursday 29 January 2026(88952)
Wed. Jan/28: JAC EOM is ready to be transported to the chamber (Elenna, Keita)

We've assembled the whole EOM assembly including the pivot base/plate assy and the strain relief post and confirmed that the EOM face/side/bottom plates are isolated from the pivot base/plate.

We've tuned the EOM such that S11 parameter at the modulation frequencies are all within 1dB of the bottom of the dip.

We still saw that the frequency shifted for 118 and 45MHz when we tapped the EOM body around, even though there was no appreciable change in 24 and 9MHz. Each jump was small, like 5kHz or 10kHz or nothing sometimes, but they jumped. Surprisingly, at least for 118MHz peak, after the frequency jumped in one direction due to my tapping on the side plate (e.g. the input side), I tapped the other side plate (e.g. the output side plate) and the frequency jumped back into the opposite direction. This was very consistent.

This means that my expectation was wrong. An expectation that somehow something (like coil wires) is caught by something else (like the core by the friction), and that tapping things will release these "something"s into lower potential state and that eventually they all settle.

Realizing this, we stopped tapping, we just tuned as good as we could and stopped.

Tools and parts were wrapped and bagged. EOM assy was wrapped in a foil. These things will be transported to HAM1 tomorrow. 

In the first two attachment, Elenna is tuning the trickiest frequency (118MHz). 

Following pictures show the fully assembled unit from the back (+Y), input (-X), output (+X) and front (-Y). In front.jpg, note that I'm only using one washer for the low profile 10-32 socket head cap screw. I used to use two, but the screw still stuck out just enough to make things tedious and inconvenient when lowering the pivot plate over the pivot base. Though the screw is 0.5" long and not the initially specified 10-32 x 0.375", with one washer it seems to work. 

Next, look at one 1/4-20 screw below the above mentioned 10-32 in caution.jpg. When tightening/loosening that screw, don't use a T-handle wrench unless it's a ball end tool, because you WILL damage the SMA connector thread. Even if you use an L-shaped tool, if you don't pay attention you can damage it. Be careful.

Last picture showcases a happy mood in the optics lab after the successful day.

Images attached to this report
Comments related to this report
keita.kawabe@LIGO.ORG - 08:36, Thursday 29 January 2026 (88954)

We modernized the measurement apparatus and used FieldFox (Agilent/Keysight's handheld network analyzer) instead of 4396B. This was really convenient and helpful because one person could hold the analyzer at a convenient position/angle for the other who was turning the trim cap.

Also it has a splitter and a directional coupler built in so there's no need to connect any such external devices, it's just the analyzer, a cable and the EOM. (But of course you still have to calibrate with short/open/load like in 4396B, see alog 88887.

corey.gray@LIGO.ORG - 08:37, Thursday 29 January 2026 (88955)EPO

EPO tagged.

elenna.capote@LIGO.ORG - 11:55, Thursday 29 January 2026 (88961)

Just want to add some notes:

  • once the EOM was mounted on the base plate, we used a multimeter to check the isolation of the EOM assembly and the base plate. There was no continuity between the sides, face plate, and bottom of the EOM and the base plate
  • the strain relief posts required different amounts and types of washers to ensure that when the posts were screwed down they faced the correct direction according to the drawing. You can see this in the third image in Keita's original alog. The left side strain relief post uses one 0.025" washer and eight 0.002" washers. The right side post uses one of the given slotted washers and one thick washer, I can't remember the size (but not one of the already-mentioned washers). Figuring out which washer combination was correct was a very annoying process.
  • For tuning: this is a very tricky process because the trim pots are very sensitive. To make this extra hard, it's important to note that just bringing the yellow tool in to connect to the washer changes the capacitance significantly, and removing the tool and your hand changes it back. This means that you have to over/undershoot the tuning while your tool is in, and then check to see if you have it right by removing the tool. This requires a lot of trial and error to determine exactly how much overshoot is required. I'll admit that I got it mostly through guessing and luck. I don't see how it would be possible to do this tuning without being right next to the EOM, so in-chamber adjustments are going to be incredibly difficult.
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