Reports until 10:50, Thursday 19 December 2013
H1 SUS (IOO, ISC)
jeffrey.kissel@LIGO.ORG - posted 10:50, Thursday 19 December 2013 (9025)
h1sushtts.mdl modified to temporarily remove OMs from USER DACKILL
J. Kissel, J. Rollins, A. Staley

In order to align the in-vac REFL path, as well as address proper spacing of the RM's eddy current damping copper block / magnets JAmie and Alexa need the RMs steerable and dampable. However, with the battles I've been having getting the HTTS model up and running, I hadn't noticed the obvious -- if we connect the OMs (whose models are down and out, and screens are not-yet functional) to the USERDACKILL, which blocks all HTTS drives (including the RMs) -- one cannot operate the RMs.

I have subsequently, temporarily removed the OM1, OM2, and OM2 inputs to the USERDACKILL, recompiled, reinstalled, restarted, and restored the h1sushtts on the h1asc0 front end. Now, the RMs can damp and actuate as desired.

Note -- I'm still not finished with the HTTS and HAUX model modifications; please bare with me in this time of flux. I hope to get through with this by the end of the week.