Yesterday Dripta & I went to the End X Station to do a TX module Maintenance.
The results of this TX Module Maint can be found here T1600436 :
| Laser SN01 | Incoming laser power from T1300100 | |||||||
| Date | 6/4/2013 | Aug. 3, 2018 | Mar. 19, 2019 | Jan-18-2024 | April-22-2025 | Jan-27-2026 | ||
| Laser Shutter Check | PASS | PASS | Pass | Pass | Pass | |||
| Max OFS Offset | 9.9 V | 7.8 V | 7.7V | 7.7V | 7.75 | |||
| 95% OFS Offset | 9.405 V | 7.4 V | 7.3V | 7.315 | 7.36 | |||
| Operating OFS Offset | 4.7025 V | 3.7 V | 3.85V | 3.6575 | 3.68 | |||
| Laser Output Power | 2.05 W | 1.72 W | 1.75 W | 1.67W | 1.7 | 1.662 | ||
| After-Laser Rejected Power | 56.5 mW | 54 mW | 36.6mW | 34.6mW | 35.7mW | |||
| AOM Input Power | 1.60 W | 1.69 W | 1.59W | 1.65 | 1.64 | |||
| Max Diffracted Power | 0.967 W | 1.13 W | 1.1W | 1.14 | 1.1 | |||
| Un-Diffracted Power | 0.359 W | 0.306 W | 266mW | 0.307W | 0.297 | |||
| AOM Diffraction Efficiency | 60.44% | 67% | 69.00% | 0.690909090909091 | 0.670731707317073 | |||
| After-AOM Rejected Power | 12.8 mW | 13.7 mW | 14.7mW | 15.2mW | 16.7mW | |||
| TxPD Power | 11.1 mW | 6.06 mW | 6.36mW | 11.9mW | 6.14mW | |||
| OFSPD Power | 5.7 mW | 6.56 mW | 6.36mW | 5.7mW | 6.58mW | |||
| Outer Beam Power | 228 mW | 0.257 W | 265mW | 0.536 | 512 | |||
| Inner Beam Power | 228 mW | 0.255 W | 260mW | 0.526 | 501 | |||
| Output Beam Power Ratio | 1 | 0.992217898832685 | 0.9811 | 0.98134328358209 | 0.978515625 | |||
| OFS Gain | 38.19 dB | 41 dB | 39.6db | 39.6 | 39.79 | |||
| OFS Phase Margin | 60.9 degrees | 55 degrees | 43deg | 42.1 | 42.3 | |||
| ALOG | 75484 | 88949 | ||||||
Jennie W, Jason O
Jason and I added four beam dumps - two before we turned the power up, two after.
There were no beams leaving the table at 100mW but we dumped two beams going towards the PSL septum plate (one was transmission through JM1).
Jason saw one leaving the table after we were at one watt so this and the transmission throuhg JM3 + JM2 are now dumped.
PSL power into HAM1 has been returned to ~100mW and the PSL rotation stage is de-energized and locked out once again.
Pictures of the beam dump positions are attached.
BD one: BD for beam reflected towards PSL from JAC (-x direction).
BD two: beam transmitted through temporary JM3, BD (right one in photo) at edge of table nest to JM1 tip-tilt (in its temporary position in bottom right of photo).
BD three: BD in bottom of picture added for beam transmitted through temporary JM1.
Photo of both BD 1 and 3 zoomed out.
BD four: BD on -x side of table (towards HAM2) catching beam transmitted through JM2, shown in mid-left of photo.
S. Muusse, M. Todd
Lens realigned on X-arm CHETA table for corrected focal lengths and the beam profiled which had better agreement with the model. ITM beam size from fit are much closer to ideal beamsize on ITM (≈ 52.7mm).
Fit for profile after L2 vs model
| Fit | Model | |
| w0x,w0y [um] | [970.5 ± 28.7, 940.8 ± 23.3] | [1023.9, 981.71] |
| z0x,z0y [mm] | [-1078.1 ± 32.0, -901.9 ± 22.5] | [1.046 , 0.928 ] |
| qx [mm] | 1.078 ± 32.0 + 0.643 ± 38j | 1.046 + 0.708j |
| qy [mm] | 0.902 ± 22.5 + 0.604 ± 30j | 0.928 + 0.651j |
| Beam radii at ITM [mm] | [54.442, 55.885] | [52.311, 54.385] |
Beam radii at ITM is foudnfrom fit by propagating the fit q to the ITM.
We commissioned the 2 whitening concentrators in the ISC-R6 rack, after some of the chassis were rearranged, see alog 88922.
The whitening concentrators control the ASC-AS_C, the OMC_A and the OMC_B QPDs, and will in the future also control the ASC-LO_A and the ASC-LO_B WFS, as well as the ASC-LO_C QPD.
The slow controls software needed to be updated to support this.
All whitening controls channels were verified using the binary IO tester.
Wed Jan 28 10:05:11 2026 INFO: Fill completed in 5min 8secs
WP12980 DAQD code upgrade.
Jonathan, Daniel, Dave:
The DAQ was restarted at 16:08 Tue 27jan2026 for Beckhoff ISC-CS changes, applied when Daniel restarted the slow controls system earlier that afternoon. This was an EDC + DAQ restart.
We took this opportunity to complete the upgrade of DAQD on the 1-leg (it has been running on the 0-leg for over a week).
the 0-leg was a standard retstart, the 1-leg was a staggered restart node-by-node to implement the upgrade, followed by a full restart of the 0-leg.
Tue27Jan2026
LOC TIME HOSTNAME MODEL/REBOOT
16:08:03 h1daqgds0 [DAQ] <<< 0-leg restart
16:08:10 h1daqfw0 [DAQ]
16:08:10 h1susauxh56 h1edc[DAQ] <<< EDC restart for new Beckhoff channels
16:08:11 h1daqnds0 [DAQ]
16:08:11 h1daqtw0 [DAQ]
16:16:15 h1daqdc1 [DAQ] <<< 1-leg restart, new daqd.
16:16:21 h1daqfw1 [DAQ]
16:16:21 h1daqtw1 [DAQ]
16:16:22 h1daqnds1 [DAQ]
16:16:31 h1daqgds1 [DAQ]
16:17:06 h1daqgds1 [DAQ]
I tested these in the morning with the Fieldfox TDR and found two of the Heliax terminations were bad on the HAM1 end of the run. I reterminated them and completed the install to the feedthrough, then took new TDR scans, they are uploaded here.
Yesterday Rahul and I went to HAM7 to try to address the suspension problems reported in 88913.
I watched the beam on SQZT7 irises in the homodyne path while Rahul moved cables away from the suspended platform, the beam moved as he shifted the cables near the V3/H3 osems (the hard to reach ones) away from the platform, but not so much that we lost the beam. He also tried lifting the cable connector for the new translation stage on and off the OPO, this had a similar impact on the alignment but we never lost the beam.
We left the connector as it was, but moved the cables away from the platform. The beam coming out of the chamber was hitting the top of the upper periscope mirror on SQZT7, clipping somewhat there. We took the power meter in chamber and measured 20-30% losses between the beam leaving the platform towards the filter cavity and the beam returning in transmission of SFI1, which was pretty consistent with the power measured on SQZT7.
Jeff re-evaluated the suspension health 88921 yesterday afternoon. This morning from the control room I moved ZM1 in pitch -1800 urad which seems to have relieved the clipping according to the OPO IR TRANS PD, but has saturated ZM1 pitch. This can probably be offloaded to A:M3 to relieve the saturation.
Closes FAMIS#38813, last checked 88386
BRS Driftmon
Auxiliary BRS Channels
Everything is looking normal
TITLE: 01/27 Day Shift: 1530-0030 UTC (0730-1630 PST), all times posted in UTC
STATE of H1: Planned Engineering
OUTGOING OPERATOR: None
CURRENT ENVIRONMENT:
SEI_ENV state: MAINTENANCE
Wind: 4mph Gusts, 3mph 3min avg
Primary useism: 0.03 μm/s
Secondary useism: 0.33 μm/s
QUICK SUMMARY:
LVEA is still LASER HAZARD
Summary:
A day of success.
How crystal mounting was done.
We did "in-between" method (alog 88900) and inserted two pieces of 3/8IDx5/8ODx0.025" thick shim washers between the front plate and the input side plate. shim_washers_spacers.jpg shows the washers and the front plate before the rest of the EOM structure is placed on top. Note that the front plate still has the alumina piece on top, not the RTP. Important points in this picture:
(Added later: If I were to do this again, I'll set the set screws with alumina piece in place such that all touch the board when there's a good contact between board/plate/alumina (of course no indium). Insertion of indium foil with the real RTP later will automatically ensure that the screws are just shy.)
Next we cut a 40mmx4mm piece of indium sheet with a clean pair of scissors and installed it in a groove in the front plate. I tried to set the edge of the sheet to be 7.6mm from the outside edge of the front panel (this is 7mm plus the thickness of 0.025" washer). Judging from indium.jpg, I was mildly successful, maybe it's more like 7.4mm but it's not 7mm nor 8mm.
rtp.jpg shows the side view of the crystal. Maybe it's hard to see but it's wedged, in this picture the shortest face is down, the longest side is up.
I placed the crystal on top of the indium sheet, making sure that the edge of the crystal is well aligned with the edge of the indium as good as I can. We also made sure that the shortest face mates with the front panel. You cannot see any of that in the crystal_installed.jpg but you can at least see that the crystal is there.
Then we went through the same procedure we've already done more than several times, i.e. tighten the screws on the input panel until the panel touches the washer and the washer touches the front panel, tighten the scrwes on the output panel so the screws touch that panel, then go balanced tightening, moving just a tiny amount at a time, always applying small downward pressure for the EOM side/board/bottom assy otherwise the assy will shift when the screws are tightened. When all of the screws are tightened stronger than finger tight, screws on the input side are tightened just a bit more. After this, neither Elena nor I weren't able to undo screws by finger.
Sorry no picture of the assembled unit.
Tuning is done, larger capacitance than obtained before with alumina, looks good. (But why do the dips have to be so narrow?)
We noticed that the frequencies were lower than what we have previously obtained with alumina, i.e. the capacitance is bigger. This is probably a good sign even though we don't know if this is due to the indium or something else. Especially, 118MHz dip was a MHz or two lower than nominal.
We were able to tune all four frequencies using trim cap, except that the trim cap for 45.5MHz hit the minimum and we could not increase the frequency any more, so we bent the winding of the coil a bit to spread loops apart. Below is the table of center frequencies (actual vs nominal). In the attached photos, cursor is placed close to the nominal frequency. They all look good in that the frequency is close enough to nominal that we're only loosing less than a dB, but the resonances are all very narrow (for my preference, anyway). The Q values are from 640 for 9MHz to 1300 for 118MHz, going higher as the frequency. A small change in frequency will result in a big degradation in the modulation depth.
(Added later: Read Valera's entry below, thanks Valera! The numbers here are not the real Q, they should be smaller. To make it more embarrassing, I somehow mixed up 3dB and 6dB. Given that all dips are smaller than -20dB, a quick thing to do is probably to define the width of the peak as full width of the -3dB points in S11, not +3dB points from the bottom but really -3dB measured from 0dB full reflection. If you do that the numbers are more like 100 instead of 1000.)
If you look at the pictures, you'll also notice that the reflection dips at the center are -23dB (9MHz), -24.5dB (24MHz), -23dB (45MHz) and is -25dB (118MHz) so a bit smaller than 10% in amplitude is coming back. It's not really matched to 50 Ohm transmission line, and that on its own is OK, but because of that, I wonder if we can add a bit of resistance to bring down Q values without any negative impact (like worse matching with increased reflections) in the future design.
| Tuned center | Nominal | |
| 9.0995 | 9.100230 | |
| 24.07705 | 24.078360 | |
| 45.5043 | 45.50115 | |
| 118.3055 | 118.30299 |
After this first round of tuning, three set screws on the front plate were all extracted, and there was no change in the tuning of 118MHz dip.
I changed the orientation of the EOM and the frequency jumped a bit
Up to this point, tuning was done with the front plate facing down and put on the ceramic insulator placed on the EOM base (because it's convenient to access trim caps that way).
When I changed the orientation of the EOM so the front plate becomes upfront (i.e. like intended), the frequency of 118MHz dip shifted a bit, from 118.3055MHz to 118.31745MHz, it's just 12kHz shift so not the end of the world but it's still meaningful. Maybe it's the interaction of the magnetic field from the coil and the metals nearby?
Then I tapped the front plate and side plates and it shifted again, fortunately by smaller amount (from 118.31745 to 118.3113MHz, a negative 6kHz jump).
What we'll do tomorrow is to fully assemble the unit, tune it again as good as we can, then tap and retune if necessary. Hopefully, tapping enough and things will settle to the bottom of the potential.
Once the EOM goes into chamber we'll measure the resonances again, and we might have to retune in chamber.
I was also wondering why the S11 (return loss) is narrower then the transmission curve back when we did the prototype testing at LLO. So I did the math myself - the attached plot shows the calculated curves for voltage across the crystal for 1 W incident RF power and S11 for 9.1 MHz (similar for other f's). Initially I also made the same mistake estimating the Q - the Q is actually about 100 not ~1000 as one can see from the transmission curve (voltage on the crystal).
Jeff, Sheila, Rahul
Details about OPO health check issues (Yaw dof. - frequencies are off and unnecessary peak observed) is currently being analyzed - see Jeff's alog 88913.
This morning we discussed about possible cable interferences in OPO.
I went into the chamber and took fresh pictures of the OPO from several angles, focusing on cable routing, cable resting on the OPO etc - please find them attached below. I will compare them with the pictures posted in LHO alog 61643 (by Sheila in 2022) and look for possible culprits (a few of them already).
Moving cables could cause some misalignment, hence we will start doing so once Sheila gives us a green light.
This afternoon Sheila and I went into the chamber and nudged some of the cables away from the OPO - Jeff will re-check the TF measurements to look for any improvements.
There is a cable connector sitting on the OPO (which is a new addition to the OPO). I lifted that cable connector and then Sheila looked for alignment shifts - which she confirmed. For now we left the cable connector at the same spot on the OPO. We will think of moving it away after Jeff's results.
Sheila also found some changes in the beam alignment since last week - not sure if this is due to our work (AOSEM re-centered LHO alog 88910) from yesterday - although centering aosem-flag should not change the mechanical alignment.
EPO tagged
J. Freed,
Continuing From 88293, I took phase noise measurements of waveform generators relevant to SPI pathfinder with two different methods. This first method is the standard method that LIGO uses which follows the BluePhase 1000 manual. I used this method to highlight the issues this method has in the context of SPI. The second method is a slight modification to the standard method which shows a lower noise floor in the area of interest for SPI.
First Method: BluePhase1000_Setup.png (from LIGO-T2400324) Shows a simplified Phase noise measurements set up of what the BluePhase 1000 manual provides. A simple way to take phase noise measurements is to mix the signal from the Device under Test (DUT) with a reference device (REF) outputting the same frequency but at quadrature. Ideally, this mix outputs only the differential noise between the two devices. If the reference device has much better performance, then the mix ideally outputs only the DUT noise. In this method, a feedback loop is used to keep the REF at quadrature with the DUT. For the REF device, I used the 80MHz OCXO housed in LIGO-D1100663.
OCXOComparisonTOCXO.png Shows the results from the first method, I used 3 different devices as the DUT; a 80MHz OCXO here at LIGO LIGO-S1000565, a SRS SG382, and a Keysight 33600A. The main thing of note is that OCXO is expected to have a much lower noise floor than any other device; however, below ~60Hz the noise is not limited by the different DUTs. Since the REF is another OCXO, I believe the feedback loop that keeps the REF device in quadrature is limiting measurements below 60Hz. Since SPI is interested in phase measurements well below 60 Hz this first method will not work for taking phase noise measurements for SPI. Especially since SPI has both an 80Mhz and an 80MHz -4096Hz signal and LIGO does not have a 80MHz -4096Hz OCXO to use as a ref.
Second Method: PhaseNoiseSetUp.png shows the modified set up; where the REF device is the SRS SG382. This method puts the REF device at quadrature by setting it manually and holding it there through the 10MHz timing port created by dividing by 8 the 80MHz OCXO signal. Since both the REF and DUT are referenced to the same OCXO (or the DUT is the OCXO itself), ideally both devices will be held at quadrature bypassing the need for a feedback loop. In practice, I did notice a small amount of drift from quadrature over time.
OCXOComparisonSRS.png Shows the results from this method. This graph shows both the OCXO and the Double Mixer have phase noise performances well below the noise performance of a typical waveform generator (Keysight) below 100Hz. Though combined with the last alog, still very much better than SPI requirments.
Difference: OCXOComparisonSRSOC.png (ignore the title on this plot) shows the mix of an 80MHz OCXO and the SRS using the two different methods to hold one at quadrature with the other. With the modified method, we are not limited as much below 60Hz, except those peaks at ~0.16Hz, ~0.45Hz, etc.. which I believe are caused by the divide-by-8, not the SRS; as the SRS measurement using the first method did not have these peaks.
Extra:
OCXOComparisonFull.png Shows all measurements on one graph.
OCXOComparisonKey.png Shows that Keysight had strange harmonics at multiples of 5kHz but disappeared 12 hours later.
Applying the equation found in 88293 to the data in the modified method, we get a new plot Keyrad3.png that shows the SPI noise budget for phase noise of oscillators used in the build/install of SPI. We can come to the same conclusion as last time, that since SPI has a reference interferometer the noise drops significantly at low frequency (the area where SPI operates). The noise from SPI's selected oscillators for the build/install is expected to have a negligible effect on our noise budget.
10-32x0.375" SHCS that was blocking the access to one 1/4-20 screw was replaced with a low profile 10-32 SHCS.
"Issue 2" in alog 88862 was solved.
See picture, Mitch found a 10-32x0.5" SHCS with a low profile head. 0.5" seemed to be OK in that it's not too long, but we used two washers to make sure that the scrwe doesn't bottom out.
EOM crystal mounting practice part 2 (with a remote help from Michael)
Summary:
Laxen method test.
In alog 88862 we left the EOM module with the alumina piece mounted using Laxen method (no gap between the input side plate and the front plate, a big gap for the output side).
Shining flashlight into the iput or output aperture in the side plates is useful to see the gap between the electrode plate and the alumina piece, and we found that there was indeed a small gap only on one side (i.e. the "crystal" was pinched at the edge).
I loosened the screws for the face plate and repeated the mounting procedure, but this time being extra careful to tighten the screws by tinier amount (than my previous attempts) at a time while applying a gentle pressure from the top. As soon as I got much tighter than finger-tight, I stopped. This resulted in what was seemingly a good contact between the alumina and the electrode, no light visible between them.
See nogap.jpg, this is a representative picture of GOOD contact (even though I cannot prove that the contact is really plane-to-plane not just plane-to-one edge of the crystal).
Another picture gap.jpg is an example of BAD contact. It's hard to see but there's no gap at either edges closer to input/output faces, the gap is only in the middle. I don't have a good explanation for this.
Appert method tests.
We also tested Stephen's suggestion to make a gap on both sides of the front plate. This was trickier but doable by using two Allen keys. The third attachment (EOMassembly.jpg) shows the EOM placed on top of the EOM mount parts just for picture AFTER the alumina was mounted. During the mounting process, the face plate is facing down, and two allen keys will tighten two screws with green (or red) arrows in the picture with tiniest rotation at a time. Green, red, green, red, repeat it until it feels reasonably tight but much, much looser than you'll usually do for tight mechanical connection. After this was done, neither Matt nor I were able to undo the screws by finger.
We did this twice, both times no gap between the alumina and the board, and alumina didn't slip out.
Output side plate might be warped?
In the assembly picture, can you see that the gap between the face plate and the output side panel (right on the picture) is uneven, but the gap for the input (left on the picture) is fairly even? I don't think this is an optical illusion. This might be related to the reason why the crystal ALWAYS slips out when the face plate is tightened down to the output side plate, see my alog (88862). Quoting myself, "no matter what we did, the alumina piece (i.e. fake RTP for excercize) slid out of the assembly but only after tightening the screws". Maybe it's the output side plate.
Reflection measurement.
For each of the above three practices (one with Laxen method, two with Appert method), S11 coefficient was measured for all four ports.
What we found was that all four reflection dips were higher than they are supposed to be. According to Michael, alumina should give us similar results to RTP. I don't list results for all three sets (3x4=12 numbers) because numbers were pretty consistent across the sets, maybe give or take 10kHz or so.
| Nominal LHO/LLO (MHz) | 9.100230 / 9.099055 | 24.078360 / 24.078 | 45.50115 / 45.495275 | 118.30299/118.287715 |
| Measured (representative number) (MHz) | ~9.17 | ~24.10 | ~46.05 | ~119.8 |
In the attached pictures, green line is roughly where the center should be. 9.1 and 24.08 look reasonable to me. Not sure about 45.5MHz, it's 450kHz off. 118.3MHz is totally, totally off.
As I wrote in the summary, I tried bending the coil windings for the 118MHz (bendandsqueeze.jpg) because it was the worst but also because it was the one with the loosest of all four coils (118MHzWinding.jpg), and it had a huge effect. With just a few rounds of bending/squeezing I was able to go down to 118.53MHz (afterbending_118MHz.jpg). I could have passed 118.3 and gone to the other side easily but I stopped there.
Just in case somebody else must do this, here's what I did to measure S11 (reflection coefficient).
If you go to the optics lab, everything is already set up like in the attached cartoon except that the dirty cable is removed from the coupler and placed on top of the optics table. You might still do the calibration again (because we turned off the analyzer at the end of the day and I cannot remember if the calibration results are kept in the analyzer). Remember that EOM is class A but your cables are dirty (even though we wiped the connectors of the dirty cable using q-tips and IPA). We're using one sacrificial SMA elbow that used to be class A to connect your dirty cable to the EOM.
Anyway, calibration. Set the frequency range to whatever you want but make sure that it covers the frequency range of main interest, like at least 9MHz to 125MHz or so while performing S11 calibration.
Connect the BNC of the dirty cable to the INPUT connector of the directional coupler, like in the attached cartoon.
Press "cal" button and select S11 calibration. Don't connect anything to the SMA of the dirty cable and press "Open" button. Next attach a hand-made short circuit plug to the dirty cable via BNC male to SMA female connector. Press "Short". Then connect a 50Ohm SMA terminator to the dirty cable via SMA barrel. Press "Load". Then press "Done".
Now you're done with calibration. Press "Measure" and make sure that you're measuring S11.
Clean the SMA with IPA and q-tip again. Connect the dirty cable to the elbow, and the elbow to the EOM. Set the frequency range to whatever you want. That's it.
Quick Monday update.
I measured S11 coeff without the crystal/alumina but with the front panel.
Reflection dips with/without alumina are:
| ~9.17/9.192 | ~24.10/24.214 | ~46.05/47.106 | ~118.53/122.736 |
So the frequencies are consistently higher without the crystal/alumina.
EPO tagged
In prep for HAM7 closeout, the temporary viewport assembly was removed from the HAM5 relay tube port. RV-1 was closed, and the volume vented with viewport covers still installed, with dry N2. I monitored the corner pressure (PT-120B) during venting, to make sure there were no leaks through the gate valve. No change in pressure, so I continued with viewport removal.
Viewport was removed first, then the pump-out tee. The mitered spool piece and bellows assembly was installed on HAM5 side. Lines were marked across the relay tube assembly prior to removal, so the install orientation remained the same.
The ported spool piece will be installed next week during Laser Safe conditions. Bellows flanges were covered with foil for protection.
EPO Tagged.
[Sheila, Karmeng]
We took a bunch of photos on HAM7 and SQZT7 today, the IR-green coalignment is fixed.
IR-green coalignment: on the iris between ZM3 and FC1 (before and after) and after AM3 (green and red overlap)
Beam position for all 3 irises placed in HAM7:
Iris 1 IR position on the iris placed between ZM1 and ZM2.
Iris 2 IR+green position on the iris placed between ZM3 and FC1.
Iris 3 IR position on the iris placed between BM4 and ZM4, with "RL" on the Thorlabs IR card placed on the iris as a reference to estimate the deviation from the center of the iris.
For 2 irises placed on SQZT7 HD path:
Iris 1 IR position on iris1 on SQZT7.
Iris 2 IR position on iris2 on SQZT7.
We also checked the IR on HAM7 QPDs path, the IR is off centered on the lens (seen from both front and back). This was roughly centered, and will be fine tuned with the picos.
EPO tagged.
Jason. JennieW, Rahul
This morning we added the damper parts to the JAC in HAM1 chamber - see picture attached. The cables were re-routed slightly so that they don't interfere with the damper.
I have finger tightened the screws of the damper for now - since no torque spec was provided and we were worried that tightening them too much might affect its position/angle.
EPO-tagged.
Masayuki and I fully tightened the JAC body mode dampers yesterday. We were only able to get the screws ~1/2 turn past finger-tight before we could no longer tighten them. No changes in JAC alignment were observed while we were doing this.
Yesterday I picked up the shipment from LLO contain the 2nd HXDS (first HXDS shipment alog87998) and related ASSEYs and brought it to the Triples lab.
Uwrapping and inspecting was uneventful, the zip ties were intact, the shock pads untripped and the humidity indicator was unchanged in color. The outer (front, back) and inner (front, back) bags were in good condition, unwrapping the suspension I found no play with the blades. All the nuts and dowel pins were tight and well seated, the ICS looks good except for it seems to be missing the HDS Intermediate Mass Fixture (D2000230-V1, s/n 08). The part is scribed as V1, on the dcc there's a V2 with two added 8-32 helicoils taps that, based on D1900352 which uses V2, I should be able to see from the front and I don't, so this is a V1 plate and not an incorrectly scribed V2. I believe these two missing 8-32 holes are where we will attach the BOSEM Mounting plate (D2000257). The first HXDS we received in November had the V2 plate. We may have to do a small rework to update it to V2, or have LLO send the V2 part if possible.
EPO tagging