Following up on the work to replace the "dripless" quick-connect fittings in the 35-W amplifier in the PSL FrontEnd laser, see Link, today I installed the new fittings in one of the spare FrontEnd lasers.
These fittings accommodate 8 mm O.D., 6 mm I.D., tubing from the outside and transition to the 6 mm O.D., 4 mm I.D. tubing that is connected to the crystal holders in the laser head.
The installation proceeded as expected and confirms that this scheme should work for the laser currently operating in the H1 PSL. We plan to do the same fitting swap in the H1 laser room next monday.
Photos are in the attached .pdf file.
While we were sitting here with the interferometer locked and no commissioning activities related to SR3, the SR3 SD osem glitched and cause the damping loop to saturate the DAC. The interferometer stayed locked.
During O2, we had simlar glitches which caused locklosses. 32328
[PeterF, StefanB, Craig, Jenne]
We tried several different levels of RF9 modulation depth. More than nominal is definitely bad, less than nominal (nominal during acquisition) doesn't seem to do a lot in DARM. Colors should be consistent across plots, eg. ref 18 is brown is -6dB from nominal for all the attached plots. Stefan has some more plots that he'll post showing correlations (or not) with various other channels.
13:30 UTC Chris S. opening inner 'High Bay' rollup. Also working on scaffold at HAM6. 15:25 UTC Chris S. done in LVEA 16:00 UTC ISI CONFIG is in LARGE_EQ_NOBRSXY 16:03 UTC ISI CONFIG to WINDY 16:04 UTC Ran RECOVER EQ 16:06 UTC Rerequested WINDY 16:15 UTC SEI back. IMC_LOCK reports 'IMC WFS not centered'. 16:18 UTC Starting initial alignment. 16:35 - 17:07 UTC Jeff B. to LVEA, staging for vent 16:45 UTC Aidan updating HWS code 16:45 UTC Karen and Vanessa to LVEA, end stations 16:46 - 16:51 UTC Nutsinee to HAM6 16:59 UTC Nutsinee transitioning LVEA to laser hazard 17:07 UTC Jeff B. to end Y 17:09 UTC Karen and Vanessa leaving end Y, going to end X 17:10 UTC Nutsinee done transitioning LVEA to laser hazard 17:10 UTC Richard, Filiberto to ISC racks by PSL 17:10 - 17:24 UTC Betsy and Jason to HAM6 17:14 UTC Daniel S. done installing chassis 17:26 UTC Karen and Vanessa leaving end X 17:28 UTC Filiberto back 17:34 UTC Karen and Vanessa to LVEA, cleaning 17:35 UTC Jeff B. back 18:21 - 19:09 UTC Daniel V. to LVEA, turning on OSA 18:22 UTC Terry and Nutsinee to ISCT6 18:25 - 18:44 UTC Charlie to LVEA to inspect scaffolding 20:06 UTC Chandra, Kyle, Gerardo back from CER, HAM6, checking HV procedure for vent 21:25 UTC Kyle to HAM6 21:25 UTC Robert to HAM6 21:25 UTC Richard to CER 22:06 UTC Robert back 22:06 - 22:54 UTC Kyle to mid Y 22:09 UTC High dust alarm at end Y DM 1. Ran dust monitor check. All report OK. 22:56 - 23:00 UTC Bubba to HAM6 23:42 - 00:06 UTC Robert to end Y to modify ESD voltage monitor 23:59 UTC Terry back
Here is another noise budget update, with measurements taken over the last several days. The main difference between this and 45036 is the improvements in the MICH and SRCL feedforward (45110), and I have updated some of the ASC injections.
The third attachment shows the noise budget sum compared to the DCPD cross corelation this morning:
This is based on only 5 minutes of data, because I was trying to avoid glitches and times when there are injections. At high frequencies, we don't have frequency noise included in the noise budget yet, which could explain part of the discrepancy between the cross corelation and the noise budget sum at high frequencies. At low frequencies we don't know what this noise is, but there are some peaks on a smooth background.
[Sheila, Terry, Haocun]
Fiber arrangement:
Feedthrough and Mode Matching Solution:
4 Irises were placed on ISCT6 for alignment references.
Terry Nutsinee Daniel
The cables for the OSA were routed through a new feedthrough panel. There are no gaps left.
The cleanroom curtains were lowered around ISCT6 and SQZT6.
Some additional information:
Here is a good reference time for Lisa: 2018/11/09 21:31:50 UTC (6220013528), reported at 80Mpc
Grazie! Plus for you!
I've started the process of offloading the last 5 months of raw minute trend data (3.1TB) from h1tw0's SSD raid to h1ldasgw0:/trend-0 spinning media (compressed ZFS file system on SATA-BOY raid). The entire copy-and-verify process takes about 3 days.
Since h1nds0 is not the default NDS for the control room, I'll skip the exporting of these data from their temporary location while the offloading is progressing.
RGA scans at vertex/corner and EY in preparation for vents next week. Filaments on both RGAs are now off.
Note these scans were taken while stations were open to beam tube.
In prep for opening the HAM6 End cap door Monday morning, the following things have been prepped:
1) Removed Illuminator housing from door - guillotine and yellow cover are in place
2) Removed Camera housing from door - guillotine an yellow cover are in place
3) Large 16' cleanroom has been moved ~2 feet East (as far as it can) to make room at door opening end
4) Scaffolding has been erected around chamber corners and top for working at height (pictures are of partial assembly mid build yesterday)
Fil Marc Daniel
We modified the spare CM board (s/n S1102622) according to E1800338 and swapped it with the existing one (s/n S1102621). This modification includes low pass filters for the DAQ readbacks, and a frequency change in the first two boost stages to 10Hz/500Hz.
These modifications improve our readbacks. Previous data is in alog 45131.
Fig 1 shows the readbacks of the modified board.
Fig 2 shows the new 10/500Hz analog boost filter. The RMS of the error signal gets reduced by ~400.
Looking at one of the higher power runs with a REFL fast gain of +24dB, IMC IN2 gain of -24dB and a REFL IN1 gain of 9dB, we can see that both error and control signal readbacks show again excess noise. The fast/in2 gains may be too high and we should try 16dB instead. Not sure what's up with the error signal readback, maybe too much in-loop gain with the additional boost.
On Tuesday access to the LHO LDAS web servers (eg ldas-jobs.ligo-wa.caltech.edu) were updated to no longer require authentication from the LHO control room workstations.
I put the lockloss triggering into the guardian, such that the PREP_FOR_LOCKING state will force it to be triggered, so we can acquire lock. Then in DRMI_TO_POP, at the same place that the individual LSC filter banks were getting their lockloss triggers set, I set the IFO trigger to look at LSC-POP_A_DC. We have had one lockloss with the triggering active, and the next lock had much smaller violin modes.
When we engaged the violin damping after we hit resonance while still locked on RF, the narrow-band ETMY mode 1 violin almost immediately rang up. So, we need to be doing a clear history on those before we start locking. Most of our usual-width filters have step responses a few tens of seconds, but this narrow band one has a step response greater than 3000 seconds. So, when we relock and turn on that damping (since we aren't doing a clear history right now) that filter still has the lockloss transient in its memory.
I've now added turning off the inputs and clearing the violin mode histories to the guardian. The inputs get turned back on in the violin damping Settings state. We've got an EQ incoming, so I don't think we'll get a chance to see this keep the modes down tonight.
Clearing the histories after the inputs are off seemed to help - we didn't ring up the bad EY mode this time. (We also hadn't been locking overnight, but the point is that not sending junk to the mode is better, and seems to prevent it from ringing up needlessly.)
Here is a comparison between the signals at the LSC-REFL_A servo now and 3 days ago. The filter for the ASC-POP quads made huge difference in the frequency range from 10Hz to 100Hz. The rms is about a factor of 2 lower due to the microseismic. This might explain the drop in RF power at this detector reported in alog 45100.
Here is the comparison between the readbacks of the REFL common mode board before and after the gain reallocation in the AO path.
The error signal shows a flat noise of unknown origin above 10Hz. The slow and ctrl signals should be identical above the 5Hz high pass in the ctrl path, but clearly are not. The gain reallocation actually made the coherence worse!
Turns out that the measurement in alog 45100 was done when RF level was particularly small but it got worse over time, just not as bad as before.
Microseism could explain the difference between somewhat smaller RF level after it got worse (right blue arrow) VS old high RF level (left blue arrow) but not the difference between particularly good (pink arrow) and old high RF level (left blue arrow).
Just by looking at the time scale, it looks as if the heating was passing through the optimal point at the pink arrow and kept going in the other direction.
Keita asked us to check the ITM HWS sensors to see if the LSC-REFL_A levels correlated with the IFO heating during the increase in power. It looks like ITMX doesn't change very much while going through the nominal point but ITMY is still trending. Recall that the ITMY CO2 level during lock acquisition is 0.55 Watts while ITMX CO2 is 0.19 Watts, not to mention that there are point absorbers on ITMY which definitely affect the overall heating spherical power fitting.
Overall, it looks as if ITMY CO2 requires about +5-10 udiopters central heating to go from the steady state to the optimal point, which corresponds to about 50-100mW of extra CO2 heating.
The numbers I used are on the TCS simulation MEDM with the central mask actuation gain for a single pass being 2.5e-5 diopters/watt.
We increased the ITMY CO2 Guardian request hot state power to 0.02W from 0W. We lost lock before we could see if this made any improvement though.
Craig, Peter, Stefan We remeasured and turned on the MICH and SRCL feed-forward. In particular, we - Moved all violin notches to the MICH and SRCL filter banks - Moved the AC coupling to 0.1Hz (in FM2 of MICHFF and SRCLFF1 FM2) so its phase influence is small. - Moved all feed-back top the ETMX. - remeasured the transfer functions and fitted the filters (in FM3 of MICHFF and SRCLFF1 FM3). - Updated Guardian to engage them. Attached are the MICH and SRCL OUT to DARM transfer function with and without the feed forward engaged. For MICH we get about x100 suppression, for SRCL about x50.
I've found that after yesterday's maintenance, REFL_A_RF9 RF monitor got significantly smaller and more stable at the same time.
Attached left is a trend before the change. In 20W lock the RF level (CH5) was going all over the place between -18 and -8 dBm.
In the middle is a trend after the change (now) in 20W lock. After an initial hike associated with powerin up, it quenched down to about -17dBm on average and the fluctuation is much smaller than before.
To the right is the spectrum comparison of RF9_I and Q, red is now and the green is before. A small part of the RF level change could be attributed to the smaller micro seismic motion, but RMS is only a factor of 1.5 or so smaller now than before.
Interestingly, a broad bump (10-70Hz or so) that was present in REFL_A_RF9_Q as well as POP_A_RF9_I is gone now. But that isn't good enough to explain the RF level change either, something should have been going on out of band.
Could this be somehow related to the change of CM-MC board connection cable from TNC-coax to 2-pin lemo twisted pair and/or the limiter (alog 45046)?
Craig is heading to the floor to redo the RF measurement (old measurement: alog 44811).
I've attached scope prints of the current RF levels. Remember the factor of 14 for the (Actual RF to demod/RF monitor pickoff) compensation.
Actual RF to demod
--------------------
REFL9pp = 210 mVpp
POP9pp = 98 mVpp
REFL45pp = 700 mVpp
POP45pp = 28 mVpp
Overall, RF levels seem reduced from before. Also attached are the RF slider settings at the time of the measurement.
Old Pre-O3 RF levels
EDIT: The RF slider now for 9 MHz is the same as it was during the old measurement, but the 45 MHz slider is 3 dB lower.
A comment on the limiter: There is a limiter in the fast path of the common mode board. It 'soft' limits the output voltage to ~3V. It is intended to limit the transients during lock acquisition. This at some time was important for the IMC to keep the FSS well behaved. It should never be engaged, once lock is acquired. For the common mode boards other than the IMC, it was never required and should be off at all times. The signal of the ifo CM board was extremely small at the fast output, so it couldn't have been limiting.
Update: alog 45132
In my post above, the 9 MHz are in the first plot, and 45 MHz in the second. REFL is green, and POP is blue. The names are in the png name itself.