J. Kissel Will post much more details and (performance / metrics of success) later, but I've balanced the ITMY L2 coils using methods described in LHO aLOGs 11392 and 9453. Former Balance: UL 1.028 LL -0.911 UR -1.091 LR 0.968 New Balance: UL 0.973282 LL -1.01098 UR -0.98898 LR 1.02728
TJ, TVo
Feeling like we should try to capture the positions of the alignment from alog-42507, we attempted center the HWS QPDS but we had an incredibly difficult time finding the beam because it was so dim returning from the ITM and the sensitivity of the QPDs were not very good. I'm not sure if this is an old issue but we eventually gave up on this. The motivation behind this was because the current position of SR3 to get the ALS green beam onto the HWS table requires that SR2's alignment to come close to railing when trying to get the main IFO beam down to HAM6. If we move SR3, we'll have to adjust the HWS injection alignment with the periscope mirrors but it is not clear how much we can compensate before we start clipping. I think the current plan is that we'll try to wait until the ISC alignment crew (Sheila+Georgia+Hang) is happy with their spot positions with respect to the y-arm and see how much SR3 adjusted can be fixed with.
One interesting thing worth mentioning is that we removed the Hartmann plate in preparation for this alignment work and noticed that the beam did not look the same as it did yesterday even though we didn't move anything. This could be due to the SR3 drift mentioned in alog-42507 and wasn't noticed because the plate was on. There's a bit more prominent clipping on the right side and the top, but I suspect this can be easily fixed by adjusting the periscope mirrors.
J. Kissel Overheard the alarm that TMSX's independent software watchdog (SWWD) tripped at Jun 14 2018, 00:06:27 UTC. Control room reports not activity. Don't know why. Regular watchdog did not trip. Transverse DOF was SUPER rung up. ISI was still isolated, showed some red in its ST2 performance matrix in RZ, but may have been reactionary. To fix: Bypassed the SWWD. Tried just turning on all damping loops by hand at their regular gains. Saw that Transverse had obviously huge control output request. Tried slowly (well, just one-at-a-time) turning on each degree of freedom besides T with normal gain. Works. Waited for a bit, still obviously large transverse motion (looking at speed dials). Turned on Transverse with much-less than normal gain (normal = -3. Started with -0.1.). Works. Slowly (increments of factors of two, every 20-30 seconds, watching the speed dials) turned up the gain back to normal. Now looks OK. QUAD looks OK. Don't have time to figure out what happened...
Gabriele, TVo
Summary: We turned on the ring heaters to test the ITMY HWS, it is the correct sign and about the right change in spherical power for the input wattage. First we input 2 Watts but the results were faulty because of SR3 drifting, then we waited till SR3 was stable and turned the power up to 14 Watts and the results were more consistent with what we expect. The compiled the overall results are here:

Details:
After we aligned HWS ITMY and felt we were close to the conjugate plane of the test mass, we started the HWS acquisition code and took new references. In order to fine tune the alignment, we also turned on the ring heater at 2 Watts (1 on the bottom, 1 on the top) and looked at the spherical power as well as the prism_x and prism_y values. As shown by the animation, it looks very badly misaligned but we found that this was due to a drift in SR3 when we were taking measurements and this threw off our results.


A few hours later we decided to energize the ring heater with higher power (7 Watts on the bottom, 7 on the top) and made sure that SR3 was not drifting too much, we saw a ratio of the Prisms_X/Y and Spherical_Power drop to about 5mm. The animation below shows that the heating pattern is much more centralized on the heater, but this is with a bad reference prior to the SR3 drift mentioned above so it still has residual heating imbalance. When we get a chance, we can try to get a good reference and redo this scan overnight. Because the heating causes changes in alignment, it might not be compatible with other commissioning tasks (alignment, locking, etc)


TITLE: 06/13 Day Shift: 15:00-23:00 UTC (08:00-16:00 PST), all times posted in UTC
STATE of H1: Planned Engineering
INCOMING OPERATOR: None
SHIFT SUMMARY:
Winds picked up late morning (& caused some dust alarms).
Variety of commissioning activities & other activities throughout the day.
LOG:
All PD for ALS Y have been normalized to their new nominal values. The dip in reflection is about 25% (with ~40% expected with perfect mode matching, see alog 42384).
The PLL ugf was verified to be around 25kHz. The PDH servo ugf was set to about 5 kHz. We are able to use 2 100Hz/1kHz boost stages. This is now the default.
Some plots of our spectra and OLGTFs of the ALS Y PDH. Calibration was done by watching free swinging PDH flashes on an oscope, which was ~500 mV peak to peak, and knowing the green arm pole is now 280 Hz, yielding volts to Hz of 1120 Hz/V. We also rephased the ALS Y PDH error signal by around 25 degrees to align along I-phase. Plot 1 is the In-loop ALS Y PDH error signal ASD. Plot 2 is the estimated ALS Y trans noise contributed from the PDH servo. Simply multiplied the PDH error signal by the new green arm pole. This is more relevant for total ALS Y RMS, which is now around 2 Hz. Plot 3 is the OLG of the ALS Y loop. As Daniel reported, ~ 5 kHz UGF.
To drive the ESD for effective bias measurements later today.
HAM & BSC CPS's looked good for high frequencies (screenshots with all plots squeezed in are attached). Closing FAMIS 6954.
At Sheila's request I have re-centered the ITMy optical lever to capture the current Y-arm alignment. The OpLev beam was well off of the QPD with a SUM of ~500 counts; it is now centered with a SUM of ~31k counts.
Topped of the Crystal Chiller with 250mL of water. (Diode Chiller was fine.)
Inspected the two filters. The one on the left (labeled "X") had a black ring on the bottom of the filter. Not sure if this was normal, so I contacted Jeff B. (this is a new type of filter and so these filters have a black sealing gasket at the bottom of the filter. So mainly look for noticeable amounts of particulates on white filter and particulates at the bottom of the container for the filter.)
Closing FAMIS task.
Troubleshooting the noise on the HAM6 corner3 CPS, see 42471. Our testing suggested that unplugging either cable from the satellite box improved the noise in the still plugged-in channel. So, the V3 was unplugged for a few hours followed by having the H3 unplugged for several hours. Nominal configuration was restored this morning.
Attached are spectra from these three periods, the platform was damped during these times. The top plot is the current nominal state showing the extreme noise on the corner3 sensors. In the middle plot, the H3 sensor is unplugged and the V3 sensor nicely trends with the other vertical channels. The bottom plot is during the time V3 is unplugged and the H3 signal mostly trends sort of with the other horizontal signals. In both unplugged tests, the remaining corner3 signal still shows higher noise at higher frequencies maybe hinting at the underlying issue.
Also looking at the time series, not shown here, the min-max peaks are reduced nearly to pre June 1 levels when one channel is unplugged.
I have a 3IFO request in so as to swap out the crate to see if there is anything in the theory that these results suggest the crate may be the problem. FYI, this is HAM6 and this ISI was built what 10 years ago? Installed and pulled from chamber, some mods made (can't remember what off hand) and then reinstalled. It has been a test piece for many things given its convenient location. Anyway, fodder.
Will Update FRS 10851
Richard, Carlos
Had to kill the processes on the server that were hanging on and restart the process. The ITM-y camera that looks at IR is now able to launch from MEDM.
TITLE: 06/13 Day Shift: 15:00-23:00 UTC (08:00-16:00 PST), all times posted in UTC
STATE of H1: Planned Engineering
OUTGOING OPERATOR: None
CURRENT ENVIRONMENT:
Wind: 12mph Gusts, 7mph 5min avg
Primary useism: 0.06 μm/s
Secondary useism: 0.10 μm/s
QUICK SUMMARY:
Daniel is working on IMC alignment.
Richard working on cameras.
APS on-site.
HAM6 ISI is tripped (looks like CPS issue---will check alog).
The following signals were measured directly from the TTFSS. The input modecleaner was unlocked for this
series of measurements.
scope_21.png shows the fastm (yellow), pcm (green) and mixer monitor (purple) signals. The case of
the front end laser was knocked with a screwdriver. In this case the NPRO PZT temporarily rails before
a short term recovery followed by it oscillating and saturating continuously.
scope_24.png is the same as described above except that there is no temporary recovery period.
scope_34.png also displays the output of the common mode servo to the tune input of the VCO that
drives the frequency shifting AOM in the PSL (magenta). For this particular trace the breadboard that
the TTFSS sits on was knocked with a screwdriver. Clearly the PZT starts railing before the Pockels
cell follows.
This scenario would be partly alleviated by giving the PZT more dynamic range by the use of a high
voltage amplifier. The PZT is capable of handling +100V or more. The TTFSS only drives the PZT with
+/-10V.
Rick / Peter
Correction For the newer Mephisto lasers, as this one is, the PZT voltage limit is +/- 65V. For older versions it's +/- 100V.
Attached is FSS FAST_MON_OUT spectrum taken at different times over ~30 minutes with the same FSS and IMC settings. From the oldest (pink) to the newest (red) trace, the oscillation changed from terrible to good-ish.
The offending peak started from about 233Hz and gradually moved to higher frequency with smaller amplitude, and in the red trace it's not a peak but a broad bump at around 260Hz or so.
If something is close to instability at ~240Hz or maybe ~65536+-240Hz or even in the vicinity of integer multiple of sampling frequency (65536 Hz), increasing the PZT range might reduce the frequency of lock losses but we'll suffer from huge frequency noise anyway.
tek00000.png shows the fastm signal (yellow) and pcm signal (cyan) as given from the TTFSS field box.
It was noticed that the pcm signal never crossed zero and always had a slightly saw tooth appearance
to it. The same two signals taken from the TTFSS board (TP10 and TP9 respectively) are shown in
scope_11.png. Clearly the pcm signal from the field box is broken. Either the differential amplifier
(N14) or the differential-to-single ended amplifier (N15) is faulty.
More to follow.
Rick / Peter
The PCM signal from the field box and recorded by the DAQ is an rms value. So, it will never be negative.
Locked on 00 and started the script at about Jun 13 2018 04:38:34 UTC (1212899932)
Lockloss after 2.5 hours.
A quick update on the external shutter installation. We are still having issues with the external shutter, so it did not get connected today as we had planned. The shutter assembly has been removed from the shutter enclosure and we are testing it in the EE lab.
Ed found the problem, the shutter was wired to the wrong polarity. So when we tried to actuate the shutter it would obviously not. This is also the cause of the blown Control Box fuse from back in April. Ed fixed the polarity issue and we tested the shutter in the EE shop; it functioned as expected. We will install the shutter during the next Tuesday maintenance period.
This issue happened because of an ambiguity in the wiring diagram for the shutter. The diagram only covered the wires that come directly out of the shutter, not the cable that is attached to the shutter assembly (see picture). The wiring diagram is being updated to add the wiring for the cable attached to the shutter.
Per work permit 7644. I updated the PLC code on h0vaclx and h0vacly to add readbacks for the new annulus ion pumps on CP1 and CP2. I got messages when restarting h0vacly that seemed to indicate that at least one variable was forced, but I was unable to determine which. I thought at first it might be PT100, but a previous alog says it no longer was. I also got error messages when scanning the bus and decided to recreate the project and try again. I did not get error messages the next time. I think the only difference was that I activated the configuration before scanning on the second attempt. I burtrestored both h0vaclx and h0vacly to 6 AM local this morning. The in-vacuum high voltage will need to be turned back on. Dave will do a DAQ restart.
Power supplies for ESD ITMY/X, HAM6 Shutter, and HAM6 PZT were powered on on 6/12/2018 around 11:00 am.
[Jenne, Gabriele, Daniel, Keita]
Once the gate valve was opened, we started work on aligning the Yarm to the green beam. Short story: green now locks nicely, we have beam coming to ISCT1, we moved BS to get MICH flashes (with the new ITMY alignment and the ITMX that we've had for a while now), which got us some IR flashes in the Yarm. Team Hartmann (TVo, Craig, Georgia) are now setting SR3 to get the green beam out onto the TCS table.
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Next up for main IFO locking is to move SR2 to get the beam back to the AS port (after the TCS team has set SR3 to get beam out to their table).
Final attachment is our current slider values.
Methodological comment on MICH alignment
After realigning ITMY to lock the Y arm on green, the Michelson alignment was changed. We were sure about the alignment of ITMY, since it was based on the arm, and decided to keep the alignment of ITMX also as a reference. Therefore the only free degree of freedom left was the BS.
The AS port was completely misaligned, so we had to use POP to look for MICH fringes. We could not see any at first, and we did not have any aligned camera on that beam either.
By misaligning either IMTX or ITMY we could see that both reflected beams were hitting the photodiode: with one mirror only aligned the power on POP was ~2 a.u., while with both beams it was ~4 a.u. Since we could not see fringes we decided to use the following procedure, which we report here for future reference
The attached pic shows the full camera frame. The beam circled in green is the ITM HR surface scattering green light back to the camera. The spots circled in red are ghost beams from the rear surface and the two surfaces of the compensation plate. The brightest spot just left of the green circle doesn't move as function of CP alignment where the others do. So, it is most likely the reflection of the ITM AR surface. It is possible to align all red-circled spots on top of each other, at which point we can see a clear etalon effect. One explanation for this picture is that the ghost beams actually hit the camera lens.
The ITM has a vertical wedge with the thick side down. According to D080657 the wedge is 0.07°(+0.03°-0.00°). Taking the largest angle, doubling it and multiplying by the refractive index, we get a ghost beam that is angled down by about 5 mrad. Even after 30m propagation this amounts to only about 15 cm separation. This doesn't seem enough to hit any camera on the Y manifold flange.
PDH locking: From alog 42384 we see that the cavity pole moved from 1.2 kHz to 280 Hz. This is close to the original expectation of 200 Hz. In the common mode board the first boost stage was used to account for the green coating error, whereas the second stage acted as a servo boost. Both are 100Hz/1kHz pole/zero pairs. We locked by disabling all boost stages and increasing the gain by 3dB. The first boost stage now acts as the servo boost. This seems to work fine, but needs a open loop measurements to confirm.
Another pic taken by the "red" camera (mounted on VP6) after it had been resurrected. As it turns out, it doesn't have the green filter installed and is also sensitive to green. None of the ghosts are visible.
Some pics from the high resolution camera taken by Jeff B. Redish stuff is due to the oplev.