Starting CP3 fill. LLCV enabled. LLCV set to manual control. LLCV set to 50% open. Fill completed in 17 seconds. TC B did not register fill. LLCV set back to 17.0% open. Starting CP4 fill. LLCV enabled. LLCV set to manual control. LLCV set to 70% open. Fill completed in 107 seconds. LLCV set back to 38.0% open.
Lowered CP3's manual LLCV's %open value to 15% down from 17%. Lowered CP4's manual LLCV's %open value to 37% down from 38%.
Attached is a graph showing the most recent 40 hours of PT120 pressure data.
I drove IM1 in yaw to look for clipping in the IO Faraday, and did not discover any strong evidence for clipping, however, my calculations show that that's not a surprising result. The beam in the IO Faraday is off center in yaw by about 8mm, but that's still enough clearance that before there is any significant clipping in the Faraday, the beam travels off of the IM4 Trans QPD. The total angle I calculated that's needed to drive the beam off of the IM4 Trans QPD is 2500 urad, and the actual amount I drove IM1 was 2150 urad, a difference of 350 urad, which might be an indication that the beam did start to clip in the Faraday, or could be error in the calibration of the alignment drive sent to IM1.
OR... that was PITCH, which is true, very little evidence of clipping. My calculations show pitch is decentered by about 2mm.
YAW, however, the range that I could drive IM1 was only 1317 urad, only half of what my calculations show would be needed to fall off of the IM4 Trans QPD, which is strong evidence that the beam is off center in yaw in the Faraday, which is consistent with my calculation that it's about 8mm decentered.
In order to fix an EPICS channel conflict between H1HWSMSR and H1HWSMSR1, I killed the HWSX EPICS softIOC on H1HWSMSR and restarted the HWS code.
The EPICS channel names are specified uniquely on each HWS machine by modifications to the environment variables of that machine in the BASHRC file.
The HWS code currently generates two sets of EPICS channels per instantiation. This is an artifact of the corner station code running two HWS on a single machine. Currently, we're running each Hartmann sensor on a separate machine. In order to avoid creating duplicate channel names on different machines, we added fake prefixes into the names in BASHRC (ITMY0 on the HWSX machine and vice versa).
However, we missed re-running the BASHRC file on H1HWSMSR (the HWSX machine). So two machines were producing channels with the prefix H1:TCS-ITMY_HWS.
So, between killing the EPICS softIOC and restarting the HWSX code, I logged into the TMUX session on H1HWSMSR and reran source ~/.bashrc
to fix the problem. The results can be seen here:
This should permanently fix the problem in TMUX. To be super-sure, I'll get Dave Barker to reboot the machine.
h1hwsmsr was rebooted at 10:43 PDT
Dave has rebooted the H1HWSMSR computer and I have restarted the HWSX code in a new TMUX session.
Moved the Seismometer a couple meters ~9 days ago. Attached are similar plots to previous looks of the ground motion in quiet and windy periods. The quiet time is 23 May at 1100utc and the windy period is 24 May at 2300utc. Not a great difference here compared to the Roam3 position, 35938, about 2 meters +Y from this Roam4 location. I might could argue that the Roam4 location shows a bit less increase in the X dof below 20mHz but this is too subtle to be significant. Bottom line, again, another location not as quiet as ITMY, during windy periods.
The attached plots show the CS wind velocity and the coherence/ASDs of the Roaming instrument (HAM5) and the ITMY.
Found IFO unlocked and set to down upon arrival. Going through alogs. Jim is running low frequency measurements on end Y ISI.
J Kissel S Dwyer
We now think that the IMC alignment wasn't the real problem, which we had suspected earlier today 36424.
Other things tonight:
Jeff K, Sheila
Here are some symptoms we have that our initial alignment is not giving an alignment that is good enough to get through the CARM offset reduction.
1) REFL power drops too early in the acquisition sequence, because the recycling gain is low and the CARM offset is smaller than it normally would be.
Guardian state |
LSC-TR_X/Y_NORM_OUT (arm power normalized to single arm lock) |
REFL power/ REFL unlocked (good enough alignment) | Refl power when alignment was too bad to lock |
CARM on TR | 1 | 100% | 100% |
CARM 15PM | 200 | 82% | 74% |
CARM 10 PM | 450 | 60% | 40% |
850 | NA | 23% |
2) AS port camera looks bad just before DHARD WFS come on (you can see misalingment modes, Jeff got a picture to attach)
3) When we switch the AS36 Matrix while offloading the DRMI ASC, the sideband build ups get better.
We are making progress, update coming later.
At my request, Apollo enlisted the services of a air balancing company [Test Comm] to test and calibrate the air flows as well as the chilled water flows at the out buildings where the HVAC Controls Upgrade have been completed. In order to have accurate readings on the new controls and to balance the systems we needed to have current flow rates. During this testing it was discovered that the chilled water flows were greatly reduced as were the fan flows causing us great difficulty in maintaining a stable temperature at the end stations. The chilled water flows were far below the chiller minimum water flow required for the chillers which is 84 GPM. We were restricted to 30 GPM. The chilled water pumps are rated at 105 GPM. The reduced chilled water flow was mostly attributed to the reduction of the motor input from the VFDs which in the case of End Y was down to 30 Hz. I increased the running chiller pumps to 45 Hz and this allowed us to mostly control the temperatures in the VEAs. If there is continued insistence on reducing the output of the motors of the chilled water pumps, perhaps we should consider resizing the pumps.
Jeff K., Dave B., Patrick T.
Explicit steps given for reference.
1. Jeff K. noted that the readbacks for the end Y ALS EPICS channels were turning white on the ALS overview screen.
2. The current time for each PLC on h1ecaty1 was still updating on the CDS overview screen (bottom left corner under Slow Controls).
3. I ran rdesktop -T 'h1ecaty1' -g 2048x1280 -x l h1ecaty1 to connect to h1ecaty1 using remote desktop.
4. I logged in as controls.
5. The IOC terminal was minimized. I opened it by clicking its icon on the taskbar (circled in attached screenshot).
6. There were no errors initially shown in the terminal.
7. I hit enter in the terminal. The error shown in the attached screenshot appeared.
8. I hit enter again. No further errors appeared.
9. I restarted the computer by double clicking the icon on the desktop labeled 'RESTART'.
10. The issue was resolved.
The following is a list of commands to connect to various Windows machines using remote desktop:
end X BRS: rdesktop -T 'h1brsex' -g 2048x1280 -x l h1brsex
end Y BRS: rdesktop -T 'h1brsey' -g 2048x1280 -x l h1brsey
corner station Beckhoff: rdesktop -T 'h1ecatc1' -g 2048x1280 -x l h1ecatc1
end X Beckhoff: rdesktop -T 'h1ecatx1' -g 2048x1280 -x l h1ecatx1
end Y Beckhoff: rdesktop -T 'h1ecaty1' -g 2048x1280 -x l h1ecaty1
Created FRS 8220.
HAM11's annulus ion pump (AIP) went railed high recently. Both the pump and the controller are new and have low hours. I hooked up a pump cart and banged on the pump with me knuckles to break up any "whiskers" that may have grown to the point of shorting between the electrodes. It seems to have now recovered.
This is a continuation of yesterday's entry see https://alog.ligo-wa.caltech.edu/aLOG/index.php?callRep=36371 It appears that the scan taken on May 8th, just prior to the vent preparations, was taken before any large gate valves had been closed. The scans that I took yesterday, May 24th, were just prior to opening the large gate valves. In order to make a meaningful comparison, I will need to take a scan with the site configured as it was on May 8th, i.e. as it is now. 1615 hours local -> I energized the Vertex RGA filament in preparation for taking a scan tomorrow. I'll use the same RGA parameters as Chandra had used on May 8th and the data generated will provide a good comparison.
I performed calibrations of both end stations this week as a target of opportunity during the pumpdown of the CS. I forgot to turn off the CW injections for End X, so the data we got is not good for calibration. I will revisit End X at a later date. End Y was successful though and the full report can be found here. In summary, the RxPD force coeffiecient is within 0.24% and the TxPD force coefficient is within 0.22% of the values used for O2 calibration.
TITLE: 05/25 Day Shift: 15:00-23:00 UTC (08:00-16:00 PST), all times posted in UTC
STATE of H1: Planned Engineering
INCOMING OPERATOR:
SHIFT SUMMARY:
LOG:
13:50 Chris S moved forklift from corner station to mid-X
14:30 Chris S traveled to EY tom remove & discard absorbant pads in fan#2 room. This was due to the Glycol leak noted in aLog from Monday. about 10 mins.
16:45 Nutsinee out to HWS table. Doing fine adjustment of Hartman Y
17:10 Travis to MX for 3IFO work
19:00 Travis back from MX
19:07 Jim and Jeff runningn LF measurements opn all 3 corner station BSCs. Jeff has changed the blends for these in a way that can't be seen in ISI config.
20:00 Fil is at EX
20:17 Sheila is heading into the PSL to perform alignemt of main beam.
20:18 Pep out to EX to make measurements
20:26 Jason and Peter are going to join the PSL enclosure party
20:36 Fil back from EX
20:40 Pep arrived at EX
20:40 Travis back out to MX. Will be craning but not over beam tube.
20:50 Nutsinee goinginto LVEA (TCS cabinet)
22:04 Jason and Sheila out of the PSL for Gabrieles talk
21:22 Pep back from EX
22:10 Kyle into LVEA
22:20 Kyle out of LVEA
S. Dwyer, J. Kissel, J. Oberling Given our problems yesterday with ALSX laser diode current surpassing an old threshold (see LHO aLOG 36381), I was reviewing whether we should accept the new higher threshold as the new normal. Here, I attach 20 day and 700 day (~2 year) trends of all four ALS laser diode's current (2 at each end). Also, here is the state of current values (a simple 10 sec average) vs. nominal and thresholds: Diff from Current [A] Nominal H1:ALS-X_LASER_HEAD_LASERDIODEPOWERNOMINAL 1.842 H1:ALS-X_LASER_HEAD_LASERDIODEPOWERTOLERANCE 0.5 (was 0.2) H1:ALS-X_LASER_HEAD_LASERDIODE1POWERMONITOR 1.863 (0.021) H1:ALS-X_LASER_HEAD_LASERDIODE2POWERMONITOR 2.041 (0.199) H1:ALS-Y_LASER_HEAD_LASERDIODEPOWERNOMINAL 1.520 H1:ALS-Y_LASER_HEAD_LASERDIODEPOWERTOLERANCE 0.2 H1:ALS-Y_LASER_HEAD_LASERDIODE1POWERMONITOR 1.430 (0.090) H1:ALS-Y_LASER_HEAD_LASERDIODE2POWERMONITOR 1.588 (0.068) As Sheila suggests, "It's not crazy that the diode current follows temperature, it's that the temperature has gone crazy over the past 20 days." However, one can see that this ALS X diode 2 current has been slowly increasing over the past 2 years, so we would have hit this threshold in a few months anyways. For now, we'll keep the new ALS X threshold at 0.5 [A] (and leave the ALS Y threshold at 0.2 [A]). Question: Is this OK? The User Manual doesn't explicitly mention a limit on the diode current, but there are several mentions of a temperature controller in section 3.4 "Recommended Operation," and perhaps the most relevant is this statement in the trouble-shooting section: "Diagnosis: The temperature controller is not able to stabilize the diode laser temperature at the given value. Reaction: Try to increase the set temperature for the diode laser slightly using the trimmer at the front panel of the control electronics unit, especially if it is set below room temperature. Otherwise contact InnoLight GmbH." Note the manual also suggests that these diodes are only under warranty for 6 months ;-). Perhaps we should check the temperature settings on this diode? The other three diodes on site have been pretty insensitive to temperature over the past year, through and including the recent HVAC upgrade. I'll open an FRS ticket.
Opened FRS Ticket 8216.
Temperature and current are used to make sure we at the correct laser frequency and far away from a mode hope region. We shouldn't change this unless there is a problem with the frequency locking. It seems to me that the nominal was always somewhat low, maybe 1.95 would be better.
The current limit is normally listed on the datasheet that comes with the laser. In this case it does not appear to be. Failing that the diode current is limited inside the power supply. So turning the knob beyond a certain point won't have any effect.