Everything appears to be "business as usual". There are very marginal downward trends in the osc pressures and amp flow.
Laser Status:
SysStat is good
Front End Power is 35.89W (should be around 30 W)
HPO Output Power is 153.9W
Front End Watch is GREEN
HPO Watch is GREEN
PMC:
It has been locked 10 days, 18 hr 36 minutes (should be days/weeks)
Reflected power = 23.33Watts
Transmitted power = 48.29Watts
PowerSum = 71.62Watts.
FSS:
It has been locked for 0 days 4 hr and 47 min (should be days/weeks)
TPD[V] = 2.786V (min 0.9V)
ISS:
The diffracted power is around 2.7% (should be 3-5%)
Last saturation event was 5 days 23 hours and 10 minutes ago (should be days/weeks)
Possible Issues:
PMC reflected power is high
TITLE: 10/30 Day Shift: 15:00-23:00 UTC (08:00-16:00 PST), all times posted in UTC
STATE of H1: Planned Engineering
OUTGOING OPERATOR: None
CURRENT ENVIRONMENT:
Wind: 17mph Gusts, 12mph 5min avg
Primary useism: 0.06 μm/s
Secondary useism: 0.28 μm/s
QUICK SUMMARY:
14:18 Kissel in early to do some more B&K hammering in HAM2
15:33 (HFD) MSA on site for Bubba
16:05 Kissel out for vent meeting
16:12 more MSA on site for RFAR testing
16:44 Gerardo is in the HAM5 area
16:55 Chandra going in chamber with Betsy and Travis - X Manifold
16:57 Travis heading out to biergarten
17:10 Betsy ou to he biergarten
17:15 Gerardo is out
17:25 Gerardo and Peter into Optics lab
17:27 Fil out to LVEA to put plastic conduit arounf fibers that were pulled on Friday
17:43 Job Shadow student on site
17:44 TJ heading out to HAM 4/5 area.
17:55 Richard and shadow student into LVEA for tour
18:08 Greg into LVEA to take measurements for TCS table
18:18 Kyle to the Y end station
18:27 Noise Eater out of range alarm
18:54 Travis out to reset the Noise Eater
19:13 I will be turning ops over to Corey so I can assist with HAM2 in-chamber work
Members of the Stochastic Group have expressed interest in magnetic coupling for estimates of Schumann Resonance coupling during O2. Automated coupling functions for all injections are not quite ready to be posted at pem.ligo.org, so we are going ahead and posting site-wide magnetic coupling functions from the August 2017 PEM injections here.
Magnetic field injections were made at multiple locations in all 3 LVEA/VEAs and electronics rooms. The LHO injection locations are shown in the first figure below and the injection locations at LLO are similar. The code (started by Julia Kruk and completed by Philippe Nguyen) used the following procedure:
1) Coupling functions (meters of DARM per Tesla) were calculated for each magnetometer (the quadrature sum of the axes), for each of multiple injections in the local area (LVEA/VEA or electronics bay). The coupling function is the DARM signal divided by the magnetometer signal.
2) The coupling functions for each injection for each sensor were narrowed down to a single coupling function for each sensor by picking the minimum coupling factor at each frequency. Selecting the minimum coupling factor eliminates excessively high upper limit coupling factors for sensors that are far from the injection and coupling sites and thus detect small fields for large DARM signals.
3) For the site-wide maximum coupling function given here, the maximum coupling factor at each frequency is picked from the coupling factors for all of the sensors on the LHO/LLO site.
Of course, site coupling will be the combination of coupling at all coupling locations within each site - this is just the largest of these at each frequency. We think that the largest coupling factor is probably a fair estimate for the site because other coupling locations with lower couplings can increase or decrease the overall coupling. But the coupling functions here could be multiplied by a factor like sqrt(2) to be conservative.
Other issues:
There was a large change in magnetic coupling during O2 at LHO, as noted in: https://dcc.ligo.org/DocDB/0144/G1701613/002/GenevaTalkSm.pdf , and we don’t know when it happened. I think that, as Schumann Resonance coupling becomes more important, we should probably push for a continuous magnetic injection at each station, like a calibration line, or at least weekly injections. Back when our magnetic coupling was dominated by permanent magnets on the test masses, it didn’t change for years. But now we tend to be dominated by coupling to cables, and this can change dramatically as electronics and cables change. After talking with Richard M., my best guess is that the change happened May 16th when the ITM ESD power supplies were changed, but that is just a guess. For S3 it might be a good idea to set up a single continuous line injection at the LHO corner station in order to better study coupling variation.
Another consideration for Schumann Resonances is the eddy current shielding due to the steel skin of the buildings. This is not included in these coupling functions because the injection was from within the building. We should measure this, but assuming it is the same as for a chamber, it would be about: 1/sqrt(1 + (f/20)^2), or a factor of 0.93 at 8 Hz and 0.55 at 60 Hz.
Philippe Nguyen, Julia Kruk, Anamaria Effler, Robert Schofield
I noticed a pressure "bump" at Y-end recently and have now confirmed that the ion pump mounted at BT port Y2-8 has been off for the past few days. Today's troubleshooting including re-enabling the High Voltage output. This resulted in power limited (700V @ 0.5 amp) energization (no ion pumping while inadequately energized). Next, the HV cable was moved to he other HV channel with a similar result. The controller-end of the HV cable was disconnected and a VOM used to measure the cable+pump resistance (2.5 Mohm, insufficient output voltage of the meter makes this test "almost" useless). The HV cable was reconnected to the controller and the pump-end disconnected. In this configuration, the controller wouldn't output HV as the cable connector shield wasn't grounded and, it would seem, the cable isn't shorted. I noticed that the pump-end of the HV cable was noticeably "warm" after applying 700V at 0.5 amps. This observation combined with the interpretation that the cable or pump-end connector aren't shorted indicates that the low resistance is internal to the pump itself. Ahhh! The fabled "whisker" theory. Monday, we will adapt a custom HV cable and use the "Big Gun" 10,000V 600 watt power supply to, hopefully, vaporize any troublesome whiskers that have formed between the electrodes.
The pump is probably in a condensing environment at times so there may be conductive buildup on the pump feedthrough or the interior of the cable connector.
I would be surprised at whisker buildup as that pump has not pumped significant gas loads.
Also, I would fake out the interlock at the pump and make sure you can get high volts on the cable alone.
Yes, I'll disconnect the pump-end connector and then ground the shield. This should satisfy the controller and get it to energize the HV output. As John W. points out, the pump-end connector shorting would explain why it was warm and is much more likely than the pump being internally shorted when considering the pumps torr*L exposure history.
(Peter K, Gerardo M)
New OFI table is suspended in cage, some components on the cage assembly were loose, they were re-torqued. The missing corner bracket was installed, and we replaced a couple of bad 1/4-20 flat head socket head cap screws.
Next, table balance and suspension damping.
What is the tan colored staining from? These are Class-A parts?
J. Kissel, C. Vorvick I've processed the data from last week's first B&K adventure into HAM2 which included the HAUX (a.k.a. HAM Auxiliary Suspensions, a.k.a. IMs or Input Mirrors) (LHO aLOG 39096). Recent efforts tightening and torquing the cage bolts to spec (e.g. LHO aLOG 38808) has helped increase the resonance frequencies and Qs of the first bending modes of cage to ~170 Hz in Longitudinal and 220 Hz in Transverse. These modes are significantly better* than those at L1. *Here, by "better" I mean well-defined, high resonance frequencies, and features are similar between suspensions. The data I use from LLO is the same as posted in LLO aLOG 3948 for IMs 1,2, and 4 from their 2012 vent, and the more recent LLO aLOG 25919 for the problematic IM3 from 2016. After discussing with Cheryl, there are several differences that elucidate this difference. (1) While LLO has used the "IO" dog clamps of several varieties (D1100640), LHO has used the champhered-ended "SUS" dog clamps (D1100641). These create a more well-defined contact point. (2) In addition, the layout of dog clamps around the base of the cage is significantly different; LHO revised the original layout, seeing how unstable the originally prescribed appeared. See table below for comparison of layouts: Current Former Original Revised Name Name Layout Layout (LLO) (LHO) IM1 SM1 D1200623 T1400742 IM2 PMMT1 D1200625 T1400743 IM3 PMMT2 D1200626 T1400744 IM4 SM2 D1200624 (not revised) Further confirming the difference -- IM4's clamping configuration does use the IO clamps, in a similar arrangement, and the frequency responses of the cage between H1 and L1 look quite similar -- in Longitudinal, but Transverse remains quite different. In light of this data, I propose two things: (1) At the earliest convenience (if there is still such convenience left), we should ECR Cheryl's improvements, implement them at LLO, and update documentation such that India gets similar benefit. (2) Now that we've stiffened up the resonances, they've become higher Q. We should consider shoving some viton in between the suspension cage, and, say, each of its black-glass cage baffles. It shouldn't need much.
IM4 would likely benefit from additional SUS dog clamps. I'm looking into where they could be installed.
I'm also looking in to options for viton.
The baffles are SiC, and it may be possible to install viton in direct contact with them, but the brittle nature of SiC may not allow for this.
A possible location for installing viton is on the stiffening plate in the cage, which has two 1/4-20 bolt holes available on all of the IMs. These bolt holes are above the SiC baffles, so not near the beam. If viton installed here can effectively damp the resonances, this would be a minimal change to the IM cages.
I've attached a couple drawings of the IM cage stiffening plate and a picture of IM4 showing the available bolt holes.
Here are pictures from my original SUS dog clamp installation on IM4, before the SiC baffle was installed.
Day's Log Of Activities:
Never closer. Another day in the tank aligning the ITMX main and reaction chains to the oplev, while simultaneously keeping all 132 potential mechanical interferences clear. COB right now and we have something still rubbing. Boo.
Also, the ITMY is mechanically rubbing somewhere too. More next week.
All Corner Station H1 ISI Coil Driver chassis were removed from their racks and modified in trhe EE lab as per ECRs E1100821 & E1300535 . These mods also include the swapping of a wire on the temp reset switch from the "normally closed" position to the "normally open" position. Also, a number of the surface mount +15VDC indicator LEDs were installed incorrectly and would not illuminate.
Chassis S1103566 in SEI rack C1 doesn't have the "keyed" 24VDC connector. It has the typical +/- 18VDC config and associated power cable.
Chassis S1103363 (HAM2) in SEI rack C2 was noted as having a -15V led not illuminated. Upon further investigation it was found to have a bad 7915 regulator which is what E1300535 was implemented to prevent.
All chassis were re-installed and are powered up. SEI team was informed. E-travelers will be updated.
Finished the last installs of the WHAM4 damping material: the C1 TMD & access walls & table top masses, the C2 V GS13 can and the C3 H GS13 can damping bands.
This was the last WHAM ISIs needing damping installs. A few photos below for the archive. Bonus photo feature: included in C1 is the Flexure Damping 'Lantern'!
Snapshot has alignment offsets for all IMC mirrors and IM1 and IM2 in the positions that produced a flashing IMC and a level centered beam to the FI.
We've been working on realignment of the ITMX QUad suspension for a few days now. However, we continued to suffer from some low vertical on the right side of the reaction chain (viewed from back) which was strange since it is the side that did not suffer the broken wire. Sometime between alignment a few days ago and yesterday the right side sagged ~1-2mm and was mechanically grounding on the non-adjustable UIM side stop. While diagnosing this, we discovered that the left side wire (which we had replaced from the break) was an older version and was too long. So, we embarked on making new wire segments in the staging building, resurrecting the jig, an o-scope and everything associated with it.
This afternoon, we replaced both top-to-UIM wire segments of issue with the newly fabb'ed ones. This involved a good WIHA tool and all of the extra catch trays installed on the QUAD in order to do the fussy upside-down-one-handed install of the wire clamps screws. A few hours later and we have the whole ITMx suspended again. We are still low on the right side, but at least we are not mechanically grounding. This QUAD always had a bit of a mis-roll counter to the main chain, so likely the full issue is at the very top stage. New TFs in the coming days will tell us if it is back to "good enough".
Upon inspection of the removed right side wire segment, we see a faint hint that *maybe* just maybe this segment of wire slipped in the clamp (the previously bent ends are straightened out flat, while they are still bent on other segments installed). This could have occured during the standard, yet jarring realignment last week.
Betsy/Travis
J. Warner, S. Appert, T. Shaffer
We had some unexpected time to work on HAM2 baffles after some FedEx kerfluffles, so Jim and I went into HAM2 with some freshly baked parts and an engineer (just in case things got out of hand). This work went really fast with the three of us and we managed to finish up PRM, the last beard baffle, align all of the panels we needed to, and then torque and cap everything. I went into the beam tube to work from there and to be the eyes to align, and of course, I wiped on my way out.
We left the table baffle that sits in front of PR3 off the table for now, but with the mounts bolted down. This way the other crews that still need to do work have a little bit of space to work and won't scratch anything, hopefully. To place this last panel will take only a minute or two so we can easily do it after the major work is all done.
Pictures to come.