Attached are pictures of the pressure regulator and barometer for the auxiliary water cooling circuit. This circuit serves the power meters and water-cooled beam dumps on the table. The pressure in the circuit was ~3.5 bar, which seems to coincide with when the regulator is fully closed. The pressure is ~2.2 bar with the regulator fully open. Useful information to have when or if we decide to remove the regulator from the cooling circuit in the quest to simplify things.
[John, Chandra]
More investigation on leak hunt of x-beam manifold. Here's what we're trying now:
In regard to GV5 not showing as hard closed on the medm screen. I looked at the Beckhoff code. It appears that I am just not seeing a change in signal (from 0 to 1) for the closed limit switch. Both the code and documentation agree that this should be LY terminal 2 channel 4. On April 8 2015 Kyle reported that GV5 hard closed (https://alog.ligo-wa.caltech.edu/aLOG/index.php?callRep=17748). I see this in the minute trends (attached). This is the most recent time I can find GV5 being hard closed from the alogs. On April 26 2016 LY was upgraded to Beckhoff (https://alog.ligo-wa.caltech.edu/aLOG/index.php?callRep=26803). I guess we should check the wiring into the Beckhoff chassis?
From minute trends, the last time that GV5 hard closed is on March 14 2016. https://alog.ligo-wa.caltech.edu/aLOG/index.php?callRep=26065
J. Kissel As instructed (see LHO aLOG 35977), Nutsinee and Corey reconfigured the ETM ESD systems in such a way that I thought might help mitigate charge accumulation while we're venting essentially immediately after we intentionally broke lock on May 8th 2017 at ~15:15 UTC. I've measured charge today, hoping to see a noticeable improvement, if not at least a change in the trend. For ETMX: We a change in the charge accumulation, if not an improvement. GOOD! for ETMY: We do not see a noticeable charge in the accumulation rate... yet! The optical lever's report of rotational actuation strength shows the effective bias voltage continues to trend negative. HOWEVER, don't yet be discouraged: historically, when we flip the bias voltage, the first data point is confusing. One needs several weeks worth of trend to confirm an accumulation rate and direction. Assuming the IFO is still down, we may take another measurement on Friday to help fill out the data set, to make sure we're doing the right thing.
Covering for Corey while he works on 3IFO at the VPW. - Jenne, Vaishali and Kiwamu working on locking IMC in control room - Aidan and TJ working on HWS in control room - Apollo working on FMCS at end X
J. Kissel Charge measurements prefer the test mass suspension's optical levers be very well centered on their QPDs before starting. As I was centering the optics manually this morning, I found the H1 SUS ETMY suspension suspiciously low (pointed down) in pitch. After some investigation, I've learned that we're taking the opportunity during the break to upgrade the EY VEA HVAC system. After trending the optical lever, the L2 OSEMs in Pitch, and M0 OSEM in Vertical, coupled with the (formerly correct?) channel for temperature, I can see some sort of obvious, large, drift in the suspension that would be easily explained by VEA temperature excursions. I merely post this as a reminder that once we get the VEA temperature back under control -- and back to the VEA's former temperature set point, we'll need to re-assess ETMY and TMSY suspension alignments. For now, I've left ETMY with its alignment centered on the optical lever.
A little more poking around reveals that the Y-End Beam Rotation Sensor also sees an effect of the HVAC upgrade's resulting temperature changes in the Y VEA. Namely, it shows / confirms the ~3 hour, +/- (1 deg F / 0.5 deg C) oscillation in temperature reported by the FMCS channel and by the ETMY optical lever (presumably the vacuum system's effective low-pass filter is filtering out this "fast" oscillation). Note, that the variance in the VEW temperature previously was only about (+/- 0.25 deg F / 0.1 deg C). Since this is seen in both the optical lever and in the beam rotation sensor, I'm quite confident that this is a real temperature swing. Further note -- the static temperature has also changed after the upgrade. We used to hold the VEA at 68.0 deg F / 20 deg C, but it appears as though the upgrade has left the VEA at 67.1 deg F / 19.5 deg C. This likely explains the long term sag / pitch of the ETM. John will write a more detailed log later, but upon pointing this out to him, he adjusted the HEATING OFFSET and COOLING OFFSET in the new HVAC control system in hopes to reduce the ~3 hour temperature oscillation. He changed the values from 1 deg F to 0.25 deg F (though the system echoed back that these are now set to 0.0 deg F). He'll work with Bubba to change the static temperature.
J. Kissel Also note that PCAL Y sees a substantial effect of the large temperature excursions seen in the VEA during the upgrade as well, indicating that there is still some temperature sensitivity left in the system, like what was seen back in January (see, e.g. LHO aLOG 34153). The gross clipping has gone away since the temperature has *mostly* recovered, but -- presumably because of the 0.5 deg C difference in static temperature, the RXPD is reporting 0.2% higher displacement than before the HVAC upgrade. Further, one can see the ~3 hour oscillation in the RX and TX PDs.
For the record I have changed two parameters in the ENDY VEA heat/cool control.
Both "Heating Offset" and "Cooling offset" were set to 1F. I reduced these both to 0.5 after discovering that the system would not accept 0.25. The setpoint is 68F (which it was before)
The control routines may need fine tuning to get back to the control level we had before this upgrade. We await the Apollo expert for this.
See the attached screen shot. An updated temperature trend is also attached and shows a response to our changes.
Without the ALS green beam leaking onto the HWS table, it is a much more laborious exercise to align the HWS beams. However, the process involves these steps:
As of today, we've injected an SR3 oscillation a few times and successfully located the HWSY return beam but not the HWSX return beam. At this point, my suspicion is that ITMX has not returned to its nominal pre-vent alignment with enough precision to get a return beam at all on HWSX. We currently have not ITM OpLevs to check this.
This morning, we are going to proceed with getting the HWSY return beam aligned while Jenne and Co. see if they can get the DRMI aligned.
We found that there was a lot of stray light on HWSX and a little bit on HWSY. Detective work and general snooping found that the beam going through the main HWS BS was hitting the rear of the BS rather than the dump behind it.
We adjusted the input alignment of the HWS beam as much as we dared, moving it away from the center of the BS closer to the top edge (in the picture shown below). More of the transmitted beam was dumped onto the beam dump behind the BS. This had the effect of reducing the scatter getting back to the Hartmann sensor by a factor of three or so. Unfortunately, should we move the beam too far across the BS surface, the concern is that the return beam from ITMX will be clipped by the beam splitter mount on transmission.
The color range in this image is about 180 counts.
The color range here is about 60 counts.
Color range is about 27 counts for HWSY.
[John, Chandra]
Valved out IP5 and IP6 from y & x beam manifolds at 10:37 am local time. With no pumping on these volumes, we will trend the rate of rise in pressure over some time today. This will give some indication of whether we have a leak or if IP6 is going bad.
TITLE: 05/16 Day Shift: 15:00-23:00 UTC (08:00-16:00 PST), all times posted in UTC
STATE of H1: Planned Engineering
INCOMING OPERATOR: None
SHIFT SUMMARY:
Cheryl not able to make it so Nutsinee, Patrick and myself will cover. Here is a log of the morning from ~7am -10am PDT.
LOG:
CP4's Dewar is being filled today so I lowered the LLCV actuator value to 34% open. The other Dewar being filled is CP6 and will automatically adjust.
I will order LN2 for CP3 & CP7 on Thursday for next week's delivery.
Lowered to 32% open.
LVEA is Laser HAZARD (transitioned yesterday).
Multiple activities are already started this morning.
We injected oscillations into the SR3 PIT and YAW and measured the return power getting back to the HWS CCDs as a function of PIT/YAW position. We located the HWSY beam fairly quickly but we're having trouble locating the HWSX return beam right now.
To be continued tomorrow ...
[Vaishali, TJ, Jenne]
In order for Team TCS to work on their stuff, we wanted to get DRMI-related optics somewhat aligned. Vaishali put all of the optics (including end stations) back to where their local sensors (OSEMs, or OpLevs if available) said they were on 7 May 2017. This gives us good-looking IMC refl flashes, but the mode cleaner isn't locking. Note that during this work, we have the IMC refl camera, but we're not seeing anything on MC trans camera. Not sure why.
I am not seeing peaks that look nice in either of the IMC trans PDs (IM1 trans or MC2 trans), even though the flashes on the refl camera look good. Also, we're not seeing nice dips in IMC REFL DC when we get flashes. We've run all of the Down guardian states, so everything should be set up the way we expect. All of the settings that I can think of look fine. We tweaked the input PZT and MC1 to get the WFS DC values back to that May 7th time, but I'm still not seeing normal-looking things on MC trans or MC refl PDs.
I just don't think the IMC refl beam is hitting the REFL PD, or for some other reason we're not getting a valid PDH error signal for the mode cleaner. Never having been on the IOT2L table before, I don't want to start just before having to leave, so we'll come back to this tomorrow during maintenance, or whenever we can.
NB: TJ is leaving the LVEA in laser hazard.
Attached is the pump down curve read from PT-120 on BSC3. We wait until the pressure reaches 1e-7 Torr via turbo before valving in IPs and opening beam tube gate valves. Extrapolating this curve looks like this will happen late next week.
[John, Gerardo, Chandra]
John wanted to spray some helium for himself, so we spun the x-beam manifold back up and sprayed all BSC7 conflats again, in addition to IP6 isolation GV and GV4 triple flange. He sprayed He at a KF connection at the leak checker and found a e-9 Torr-L/s range leak, which could have been what Kyle and I detected last week while testing GV7.
John noticed the BSC7 annulus ion pump's reading on front display was not clear i.e. the green LED lights were fading into 6 mA + range rather than clear-cut lit vs. non lit. He tapped on the pump and power cycled the controller a few times. It seems to be reading clearly now at 2 mA. We thought if there was an internal o-ring leak and the annulus ion pump wasn't working properly, that annulus space could be the source of pressure rise in x-beam manifold. We connected an aux turbo cart to that pump and accidentally partially vented the annulus space and then pumped it back down. No change in volume pressure though, which leads us to believe that there is no internal o-ring leak. The AIP is pumping on its own again at 2 mA.
We left the x-beam manifold turbo running and valved out for the night. IP6 is valved back in. While IP6 was valved out during leak checking, its power supply read 172 uA. When valved in, it reads 520 mA. IP5 on y-beam manifold reads about 90 uA (valved in), so we still may conclude that the reason for the pressure rise in x-beam manifold when isolated compared to y-beam manifold is due to difference in IP pumping speed. When IP6 is valved out, we expect it to read even better than IP5 valved in. One thing we didn't check is the IP flange above the gate valve. We should leak check that flange while the IP is valved in. We've sprayed it a few times now, but we always keep the IP valved out during leak checking. When IP is reopened we detect some He in -9 range (no surprise), but.....
I just sprayed IP6 valve with balloon helium (because we burned through three bottles of lab helium) with it valved into the main volume and leak checker backing the turbo pump. No He detected (IP could be pumping it all away?) beyond the 5e-9 Torr-L/s steady rate that the IP puts out, but did notice the current on IP6 was much higher after spraying, rising up to 688 uA. I will check it tomorrow morning to see if it settles back down to 520 uA. Because we're using a new controller, we have yet to wire it to CDS for remote monitoring (different configuration than the old style supplies).
Turbo valved out for the night.
This morning IP6 power supply was back down to 545 mA. John watched it while I sprayed He at the IP flanges. No change.