Sat Jun 07 10:05:59 2025 INFO: Fill completed in 5min 55secs
Erik, Dave:
Web ndscope trends stopped updating around 09:45 this morning. Some nomachine sessions are having issues.
We are investigating.
I'm running the web ndscope trends on cdsws33 while opslogin0 is having issues.
Opslogin0 is reporting an ldap failure.
I rebooted opslogin0 about 12:10 PST and it's seems to be working normally.
Gerardo, Travis, Randy, Janos Today we executed WP 12595, reventing, troubleshooting, closing, and re-pumping HAM1. The times of the operations are approximate. 08:00 - 08:30: GV1 and GV2 large gate valves have been closed. HAM1 turbo and Ion pump (IP13) have been valved out. The annulus IPs have been switched off, the annulus volume has been vented. Also, IP3 was valved in to the corner, after the successful troubleshooting yesterday (see aLog 84826). 08:40 - 09:53: The chamber was vented with bottled Nitrogen. Approximately 2 full bottles were needed. Only metallic parts were used between the venting port and the bottle (no plastic tubes), and the tube was flushed with Nitrogen beforehand. 10:00 - 10:40: The Y+ door has been taken off. The O-rings have been inspected, then removed. A human hair was found at 6:30 o'clock, and a little piece of white tape was found in the O-ring's groove at 8:00 o'clock, and overall, the O-rings and grooves were substantially dirty. Pictures about these in the comments. Also, the cleanroom was needed to be moved Y+ direction, to give enough room for the forklift. 10:40 - 11:40: Chamber work. During this time, Randy stayed with the forklift, so the door was hanging from it all the time, and inside the cleanroom. 11:45 - 13:30: O-ring installation: it took a few tries, but both O-rings were installed nicely. Then, installing back the door: smooth process, with shoving it in as the last step, to avoid the O-rings falling out. 13:20 - 13:50: Pumping of the annulus systems, and roughing the chamber. The HAM1 side annulus needed ~10 mins to go below the pressure it reached in the last 2 weeks, so the troubleshooting was very successful! The roughdown goes well, too. 16:15 - 16:45: Transitioning to turbo
Because of the safety concerns of the high amount of Nitrogen in the chamber after venting, and then opening the door, Oxygen sensors have been used during the door opening process. Moreover, because of these same reasons, and because of the lack of purge air, a crossflow from a HEPA-filtered fan was also used (additionally to the cleanroom's HEPA fans), when the chamber was open.
Left HAM1 with SS500 cart pumping, it was able to reach 5.0X10-05 Torr, at such pressure the cart system will allow the interlock to be engaged, this interlock is there to protect the chamber in case of an anomaly (power interruption, component failure, etc.) and its function is to close two valves on the cart. HAM1 pressure when I left the site was a bit higher than the cart, 6.1X10-05 Torr. Pumpdown appears nominal.
The annulus for HAM1 and HAM2 are doing good. HAM1 was at 2.66x10-05 Torr, and the pressure on HAM2 annulus was at 7.57x10-06 Torr.
Plot comparing the current vs the previous pumpdown. Blue trace is the current pumpdown.
WP12596 ADF VCXO IPC between IOP-LSC0 and OMCPI
Daniel, Vicky, Kevin, EJ, Erik, Dave
New h1ioplsc0 and h1omcpi models were installed to add two IPCs at 64kHz rate between lsc (sender) and omcpi (receiver)
H1:FEC-7_IPC_IOP_PCI_ADF_VCXO_COS
H1:FEC-7_IPC_IOP_PCI_ADF_VCXO_SIN
After the new models were restarted we noticed that the new receivers were flashing with a single RX error (1 out of 65536 in that second) every few seconds, randomized between the two new channels.
At this point we upgraded h1omc0 from RCG-5.3.0 to RCG-5.5.0, the new system has code to correct for such receive errors. Erik had the new 5.5.0 boot server ready to go, it is h1vmboot5-5 (a new naming scheme).
This required the rebuild and restart of all the models on this frontend (h1iopomc0, h1omc, h1omcpi). The new RCG added slow channels, so a DAQ restart was required for all these models.
The builds on RCG-5.5.0 use EJ's new rev-lock system, whereby all the source code (mdl and C) must be committed to subversion, and only the locked revision of these files are used to build the model, not what happens to be in the userapps models directory at the time. This worked like a charm.
Later Vicky added some filtermodules to h1omcpi, which required a second restart of h1omcpi and the DAQ.
WP12597 Quarterly reboot h1guardian0
TJ
TJ rebooted the guardian machine, it came back with no problems.
WP12603 HEPI HAM1 model cleanup and removal of TT-L4C IPC senders, switch SEI-PROC to ISI HAM1 GS13 IPC
Jim, Erik, Dave:
New h1hpiham1 and h1seiproc models were installed with no problems. DAQ was restarted, both models had new INI files.
Move HWS data from h1hwsmsr local RAID to /ligo NFS
Erik, Dave:
Erik reconfigured the HWS machines to mount /ligo/data/hws as /data locally. Some files needed to be copied to the new location before the HWS cameras could operate and write current files to the new location. Archived data is being transferred to preserve lookbacks.
DAQ Restarts (plural)
Erik, Dave
Restart 1
11:02 DAQ was restarted for two changes, first the expected changes to h1ioplsc0 and h1omcpi. Second for the unexpected upgrade of h1omc0 to RCG-5.5.0 which added channels to h1iopomc0 and h1omc, and additional channels to h1omcpi.
Clean restart except GDS1 needed a second restart
Restart 2
13:52 DAQ was restarted for the h1hpiham1 and h1seiproc model changes.
Clean restart except GDS1 needed a second restart
Restart 3
14:33 DAQ was restarted for additional change to h1omcpi.
Clean restart except, you guessed it, GDS1 needed a second restart
Note that the Vacuum upgrade which would have required a DAQ restart did not go ahead today.
CDS Overview is showing h1omc0's new RCG-5.5.0 as a dark green tag. Reminder that h1susex is at RCG-5.3.0 (LIGO-DAC) and everything else is RCG-5.1.4
h1omc0 models' rev_lock revisions summary (recent changes in bold):
h1iopomc0:
22838 cds/common/src/MAX_MIN_CALC.c
24547 cds/common/src/STAT_CALC.c
30625 cds/h1/models/h1iopomc0.mdl
27113 isc/common/models/LSC_TRIGGER.mdl
h1omc:
26004 cal/common/models/CAL_OSC_MASTER.mdl
6334 cds/common/models/FILTBANK_MASK.mdl
6334 cds/common/models/SCHMITTTRIGGER.mdl
18154 cds/common/models/TRIG_RAMP.mdl
18648 cds/common/src/RAMP_VALUE.c
4225 cds/common/src/wait.c
22840 isc/common/models/FILTBANK_TRIGGER.mdl
27113 isc/common/models/LSC_TRIGGER.mdl
18148 lsc/common/models/lsc.mdl
30547 omc/common/models/omc.mdl
30548 omc/h1/models/h1omc.mdl
h1omcpi:
24137 cds/common/src/BAND_SELECTION.c
24174 cds/common/src/FIXED_PHASE_OSC_WITH_CONTROL.c
24176 cds/common/src/LOW_FREQ_DEMUX.c
24176 cds/common/src/LOW_FREQ_MUX.c
31648 omc/h1/models/h1omcpi.mdl
31645 sqz/common/models/FC_LIB.mdl
26600 sus/common/models/PI_MASTER_V2.mdl
TITLE: 06/06 Day Shift: 1430-2330 UTC (0730-1630 PST), all times posted in UTC
STATE of H1: Planned Engineering
INCOMING OPERATOR: Corey
SHIFT SUMMARY: We're pumping back down on HAM1.
LOG:
Start Time | System | Name | Location | Lazer_Haz | Task | Time End |
---|---|---|---|---|---|---|
14:14 | ISC | TJ, Camilla | LVEA | N | ISCT1 move, TJ out 15:08 | 15:16 |
14:15 | FAC | Kim, Nelly | LVEA | N | HAM1 cleaning in | 15:31 |
13:59 | OPS | TJ | LVEA | N | Transition to upgrade laser safe | 14:05 |
14:42 | FAC | Richard | LVEA | N | Check in on HAM1 work | 15:00 |
14:47 | VAC | Mitch | LVEA | N | West bay, viton search | 15:00 |
14:57 | VAC | Travis, Janos, Randy | LVEA | N | HAM1 door removal/work | 21:19 |
15:10 | VAC | Janos | LVEA | N | Door removal | 18:31 |
15:22 | OPS | TJ | LVEA | N | Check in with VAC team | 15:27 |
15:36 | OPS | TJ | Garb room | N | Checks | 15:46 |
15:46 | VAC | Gerardo, Fil, Mitch, Randy | LVEA | N | Door work, Mitch & Fil out 17:15, Gerardo out 18:16 | 19:19 |
15:51 | SEI | Jim | LVEA | N | Lock HAM1 HEPI | 16:09 |
17:10 | ISC | Camilla | LVEA | N | Install camera on ISCT1 | 18:01 |
16:00 | SAF | Richard | LVEA | N | Check on HAM1 work | 16:20 |
17:01 | SAF | Richard | LVEA | N | Check on HAM1 work | 17:44 |
17:08 | ISC | Matt, Bin | Optics lab | LOCAL | CO2 check and disassembly | 18:08 |
17:17 | FAC | Kim, Nellie | LVEA | N | Tech clean checks | 17:44 |
17:20 | CDS | Patrick | Office | N | VAC Gauge work LY -> LX | 20:01 |
17:22 | ISC | Keita | LVEA | N | ISCT1 remove old WFS X parts | 19:38 |
17:22 | ISC | Daniel | LVEA | N | ISCT1 work | 18:08 |
17:23 | OPS | TJ | LVEA | N | Check on progress | 17:49 |
17:42 | OPS | TJ | LVEA | N | Check on HAM1 | 18:57 |
17:49 | SEI | Jim, Robert | LVEA | N | HAM1 TF prep, add viton to periscope, locking isi | 18:56 |
18:24 | SAF | Richard | LVEA | N | Check on progress | 18:37 |
18:25 | PSL | Rahul, Rick | H2 PSL room then optics | N | Grab parts | 19:36 |
18:53 | SAF | Richard | LVEA | N | Safety checks | 19:13 |
18:54 | CDS | Erik | Office | N | HWS work | 19:47 |
19:00 | VAC | Gerardo | LVEA | N | Join VAC team, doors back on | 21:38 |
19:03 | VAC | Mitch | LVEA | N | Put parts away | 19:09 |
19:37 | PSL | Rick | Optics lab | N | Put away parts | 19:55 |
19:50 | OPS | TJ | LVEA | N | Check in with VAC team | 19:55 |
20:27 | OPS | TJ | LVEA | N | Talk to VAC team, maybe move ISCT1 back | 21:16 |
20:33 | ISC | Camilla, Georgia | LVEA | N | Move ISCT1 back | 21:15 |
20:57 | SAF | Richard | LVEA | N | Safety checks, ISCT1 wiring with FIl | 22:08 |
21:07 | SEI | Jim | LVEA | N | Unlock HEPI HAM1 | 21:18 |
21:30 | ISC | Sheila, Vicky | Optics lab, East bay | N | Check out stuff | 22:44 |
21:51 | ISC | Camilla | LVEA to optics lab | N | Get big ameristat bag | 22:28 |
22:15 | ISC | Keita | MIds | N | Store parts pulled from ISCT1 | 22:52 |
22:22 | SAF | Richard | LVEA | N | Safety checks | 22:26 |
23:04 | CAL | Francisco | PCAL lab | LOCAL | Open apertures | 23:13 |
Busy day, work completed includes but is not limited to:
Transition LVEA to Laser Safe for Upgrade Period permit
GRD restart (TJ) alog84854 // permit
OMC and LSC model restarts with DAQ restart 1 (CDS team) alog84861 // permit
HWS file work (Erik) alog84865 // permit
HAM1 door prep (including ISCT1 move, alog84850 // permit), removal (VAC team plus many others) permit, and reinstallation
ISCT1 work - new camera and old parts removal (Camilla, Keita, Daniel, Fil) alog84866 // permit, periscope damping with viton (Jim, TJ, Robert) alog84868
h0vaclx unsuccessful alog84871
HAM1_HEPI and SEIPROC model restarts and DAQ restart 2
WP 12577 I tried unsuccessfully to use the PowerShell scripts to generate the new h0vaclx TwinCAT 3 solution that adds the BCG552 gauge to HAM1. We are reverting back to using the voltage readout into the ADC on h0vacly. I think the most viable path forward may be to install Visual Studio 2019 onto h0vaclx or see if we can use the TwinCAT remote manager to configure and control the PLC on h0vaclx from another machine. If the second option can work, then I think it may be the best. This was done on h0vaclx: Updated WinSCP to 6.5.3. Downloaded and copied the Inficon Trigon BCG552 EtherCAT ESI-File to C:\TwinCAT\3.1\Config\Io\EtherCAT. Tried and failed to generate a TwinCAT 3 solution from the new PowerShell scripts. Exported the current version of the library code in git to PLCopenXML and imported it into a new Visual Studio 2010 solution on h0vaclx. Built the solution, saved it as a library, and installed the library file into the TwinCAT 3 Library Repository on h0vaclx as version 2.0 (version 1.0 is being used in production) Tried and failed again to generate a TwinCAT 3 solution from the new PowerShell scripts.
Craig mentioned yesterday that we might want to walk our IMC uncontrolled degree of freedom: the spot position on MC1 and MC3. I made a short script which should step the sliders of MC1 and MC3 in the correct configuration (differential step in pit, common step in yaw). If you want to run it is in
/ligo/gitcommon/labutils/imc_walk
To step both mirrors by eg 0.1 microradians, run python walk_imc_dof_4.py P 0.1
This might not end up being used since Robert suspects much of our jitter could be caused by the multiple roughing pumps running in the LVEA.
I noticed that the LLCV is railing at its top value, 100% open, it can't open no more. This is a known issue, but it appears as if the valve is reaching 100% sooner than expected, meaning when the tank is almost half full. First, I'm going to try a re-zero the LLCV actuator and await for the results. First attachment is a 2 day plot of LLCV railing today and yesterday. The second plot is a 3 year history looking at the tank level and the LLCV, it rails at 100% a few times.
BURT restore? PID tuning ok? CP2 @ LLO PID parameters attached for comparison.
Thanks Jon. However, this system has a known issue, it turns out that the liquid level control valve is not suitable for the job, that is the reason why it reaches 100% sooner than later, but it appears as if something slip, now it reaches 100% at a higher level, this is the reason why I want to re-zero the actuator.
Attached is the Fill Control for CP7 The issue was mentioned here for the first time aLOG 4761, but I never found out who discovered this is only briefly mentioned by Kyle. Another entry on aLOG 59841.
Dirty solution of solving the issue with the LLCV getting railed at 100% open, we used the bypass valve, opened it up by 1/8 of a turn and that did the job. Not a single shot, but eventually we settle on that turn number. PID took over and managed to settle around to 92% open for the LLCV. Today we received a load for the tank for CP7. We are still going to calibrate the actuator.
Bin Wu, Julia Rice
We have been working on writing a new Guardian script that will allow us to switch off the dither loops sooner in the power up process and instead use cameras.
We first looked at the error signals in the ASC cameras to see if we could adjust offsets to better values. We did this for the CAMERA_SERVO guardian, and added new intermediate states, including TURN_ON_CAMERA_25W_OFFSETS and TURN_ON_CAMERA_MOVESPOTS_FIXED_OFFSETS. We've attached screenshots showing the graph before and after our additional states. Below are the values we used for offsets for each. The weight from DITHER_ON to TURN_ON_CAMERA_25W_OFFSETS is set to be 10.
TURN_ON_CAMERA_25W_OFFSETS
PIT1 | -233 |
PIT2 | -168 |
PIT3 | -217 |
YAW1 | -248 |
YAW2 | -397 |
YAW3 | -338 |
TURN_ON_CAMERA_MOVESPOTS_FIXED_OFFSETS
PIT1 | -232 |
PIT2 | -159 |
PIT3 | -226 |
YAW1 | -248 |
YAW2 | -431 |
YAW3 | -351 |
We also adjusted the offsets for TURN_ON_CAMER_FIXED_OFFSETS:
PIT1 | --230 |
PIT2 | -181 |
PIT3 | -226 |
YAW1 | -245 |
YAW2 | -418 |
YAW3 | -353 |
These are added in lscparams.py. We also added the necessary code into CAMERA_SERVO.py.
We also added a parameter in lscparams.py for new ADS camera CLK_GAIN at 25W ('ads_camera_gains_25W', screenshot included)
Right now the new states are not requestable, so they will need to be ran manually to test. We haven't made any change to the ICS_LOCK guardian.
Also added lines in CAMERA_SERVO.py under DITHER_ON to check if ISC_LOCK is at 25W when proceeding through self counter loop, see attached.
Adding A2L gains for reference, first chart clarifies dither loop actuators and cameras.
Beam pointing actuator | ADS Dither | Cam Sensor |
PRM PIT | Dither ITMX: ITMX P2L | BS Cam 1 PIT |
PRM YAW | Dither ITMX: ITMX Y2L | BS Cam 1 YAW |
X SOFT PIT | Dither ETMX: ETMX P2L | ETMX Cam 2 PIT |
X SOFT YAW | Dither ETMX: ETMX Y2L | ETMX Cam 2 Yaw |
Y SOFT PIT | Dither ETMY: EMTY P2L | ETMY Cam 3 PIT |
Y SOFT YAW | Dither ETMY: ETMY Y2L | ETMY Cam 3 Yaw |
GRD State | A2L Gain | Cam Offset |
POWER_25W [506] | P2L ITMX: -1.25 | -233 |
P2L ETMX: 0.85 | -168 | |
P2L ETMY: 0.85 | -217 | |
Y2L ITMX: 0 | -248 | |
Y2L ETMX: 0 | -397 | |
Y2L ETMY: 0 | -338 |
GRD State | A2L Gain | Cam Offset |
MOVE_SPOTS [508] | P2L ITMX: -1.8+1.0 | -232 |
P2L ETMX: 4.0 | -159 | |
P2L ETMY: 3.6+1.0 | -226 | |
Y2L ITMX: 2.1 | -248 | |
Y2L ETMX: 4.4 | -431 | |
Y2L ETMY: 2.2+1.0 | -351 |
GRD State | A2L Gain | Cam Offset |
MAX_POWER [520] | P2L ITMX: -0.54 | -230 |
P2L ETMX: 3.31 | -181 | |
P2L ETMY: 5.57 | -226 | |
Y2L ITMX: 3.23 | -245 | |
Y2L ETMX: 4.96 | -418 | |
Y2L ETMY: 1.37 | -353 |
Today at ~11:10 am, IP3 (LVEA 2x 1250 l/s IP) failed leading to a slight pressure rise in the corner. Seen on all LVEA pressure gauges (BSC2, HAM6, etc.). Attached snapshot shows the two pumps behavior at the time of failure, pump ion current on left column, output voltage on right.
Gerardo and I went to the mechanical room to diagnose the controller, upon arrival both channels on the Dual Vac controller had tripped off. We reset the high voltage and powered on the IP. Channel 1 (corresponding to Pump A in CDS) would only reach 300 V and then would trip the controller. Channel 2 (Pump B would reach 7kV no issue but would trip when Channel 1 tripped). We then swapped to a Gamma MPC controller to test if the controller was the problem. We saw the same exact behavior where Pump A would only reach 300V and Pump B was ok at 7kV.
We then swapped back to the DualVac controller after confirming it was not the issue, but with only Pump B connected and powered on. We are continuing to monitor to make sure Pump B remains steady. In parallel, Travis and Mark are testing the HV cable to the pump to see if there are any shorts. Results to follow.
If the cable is not the culprit we will HiPot the pump to see if there are any shorts, pump will be isolated from main volume during this test. To be continued.
Using the Agilent FieldFox N9912A we measured the cable length with the following parameters:
Mode = DTF (VSWR), F_Start = 2.0MHz, F_Stop = 450.0MHz, Points 801, Resolution 261mm
Start Distance 5.0m, Stop Distance 170.0m
The cable end was detected at 80.79m from the start of the launch cable, launch cable was about 1m.
The cable measurement was similar to the other cables measured.
When measured with the DMM, this cable measured open, but when the connector was moved, it displayed ~6M ohms, this would normally not be an issue, but due to the high voltage in this location it may be an issue, recommend hipot.
M. Pirello, F. Clara, G. Morenao, T. Sadecki, J. Vanosky
Problem solved, see in aLog 84826
Daniel, Kevin, (Erik, Dave), Vicky
Kevin is interested in taking ADF sweeps around the second higher order mode arm resonance near 10.4 kHz.
We (Daniel) made model changes in h1ioplsc0 and h1omcpi that should enable higher freq ADF demods. Daniel built the models successfully. Then Dave also built these models successfully for the custom RCG running on h1omcpi for the variable duotone. We put in a WP to boot in these changes to h1ioplsc0 and h1omcpi next Tuesday 6/10.
From h1ioplsc0, we added 2 new PCIe channels to write the digital ADF LO oscillator out to PCIe. These are H1:IOP-PCI_ADF_VCXO_{COS,SIN} in screenshot 1. We also changed a rogue limiter such that the ADF should be able to scan +/-1 MHz according to the PLL.
In h1omcpi, we use the fast 64 kHz OMC PI user model to do a fast digital demodulation of the OMC_DCPD_SUM signal using the above ADF-LO PCIe channels. This is beating the fast dcpd output signal (H1:OMC-PI_DCPD_64KHZ_AHF), against the ADF LO's cosine and sine components from PCIe (H1:IOP-PCI_ADF_VCXO_{COS,SIN}), to get the demodulated ADF I/Q signals. The demod signals will have names like H1:OMC-PI_ADF_DEMOD_{I,Q}. Screenshots 2-4.
Operationally nothing should change for the ADF or for OMC-based fast PI damping. We are just using PCI to send 2 IPC channels from an IOP model to a user model on a different computer at ~65kHz, and doing the demod in a 64kHz user model (but the demod does not go anywhere, it is just used for squeezer diagnostics).
Model change summary:
h1ioplsc0
+2 IPC senders to H1.ipc
+2 slow channels to DAQ
h1omcpi
(+2 IPC receivers)
+33 slow channels to DAQ
Model changes today seem relatively successful. No way to verify in hardware (yet), but the ADF PLL claims it successfully locks at -11kHz from carrier, so at least the limiter fix in h1ioplsc0 seems to work; in principle the ADF sweep limiter is now set at +/- 1 MHz.
I added a quick ADF demod of the 64kHz OMC DCPD SUM channel into the normal ADF screen, screenshot attached, see the very bottom. New filter banks initialized with values and filters as in the other adf demod chains. Also tried to clean it up in SDF: channels are initialized, gains and phase are monitored, and saved into sdf (h1omcpi model).
J. Freed,
Spur Problem
As discussed in part 1, the Double Mixer has good phase noise around the carrier frequency to about a 100Hz out where SPI operates, however, it also has signals every 4096Hz away from the carrier. I had assumed that it was an issue relating to phase and amplitude mismatch on the phase delayer, but after adding attinuators to correct the missmatch, it helped, excepecially the 80Mhz + 4096Hz signal saw a ~15dB improvement. DM_Att.pdf. However, the double mixer still has large signals and the largest did not change with the addition of the attinuators.
I realize now that the problem lies with the mixers themselves as by the nature of a mixer they create spurs on the output.
DM_Mixer.pdf Shows the output of a single mixer. Along with the expected 80MHz - 4096 Hz and 80MHz + 4096 Hz there is extra peaks which i believe is caused by the Spurs of the mixer. The largest spur is at 80Mhz + 12,288Hz. This spur is actually in phase with the main signal and is thus construtivly interfered at the power combiner.
I do not know how to get rid of this spur as it is so close to the main carrier signal. For fun, I used a combination of Marki LC filter Design Tool and LTspice to simulate adding a filter to the end of the system to reduce the 80Mhz + 12,288Hz spur, but even an 8th order elliptical filter would only reduce the spur by ~0.04dB due to how close it is to the main signal. For fun I went to 20th order elliptic and it only reduced it by ~0.1dB. In addition, with nonstandard parts for a 20th order elliptic it got reduced by ~4dB. I am unsure of any other method to reduce the spur.
Double Mixer is a Single Sideband Mixer
I realize now that the basic design of the double mixer actually exists and is fairly common, it is called a Single Sideband Mixer (SSB mixer). Thanks to Brian, who gave me one of these mixers to test, I have something to compair the results
DMvsIRM.pdf Shows a plot of the double mixer vs a SSB mixer. The SSB mixer is tuned to 80MHz+4096Hz as apposed to the Double Mixers 80MHz -4096Hz but comparisons can still be made. For starters, the double mixers 80Mhz+4096Hz sideband equivalent is much better in the double mixer vs the SSB. However this comes at the cost of the 80Mhz+12,288Hz sideband equivalent which is much better in the SSB. In summary, just based on this single graph, the double mixer is more likely to be better for SPI for 2 reasons. One, we have already found out that SPI would be senstive to the 80MHz+4096Hz sideband equivalent. And two, if there is a way to attinuate these spurs by filtering, the spur further away from the carrier could be more easily attinuated.
High order modes filtering
Ive already discussed that adding fliters does not help the area around 80MHz. However, it does help with higher order modes
DM_Filter.pdf Shows a plot of adding a MC80-10-4AA bandpass filter from Lark engenering that has a bandwidth of 10MHz and a center of 80MHz at different positions in the Double Mixer. The best place to put one seems to be just before the amplifier, not entirly sure if adding one is nessisary to SPI but it should be good for reduceing a possible noise source.
High-Order Mode Filtering
The MC80-10-4AA that I listed actually filters by reflections, which is not helping to remove those signals from going back into the mixer. If a filter is going to be added, something like the ZXLF-K151+ would work much better.
I now realize a filter should be unnecessary as the AOMs are expected to have high insertion loss at frequencies not around 80Mhz, AOM-Tuneability.png, basically acting as a band-pass filter anyways.