Summary:
After swapping a few electronics that we broke while investigating the ALS glitches at EY, the glitches are still there, but not nearly as bad as they were. We have had these glitches go away on their own before when nothing was done, so that might be what is happening. Now they are at End X, and about as bad as they were at End Y for most of the week. ALS still will not lock for longer than 10 minutes. It might be that this problem will go away on its own, but will probably come back again.
Things that are not the cause of glitches at EX:
From PLL bypass test:
Other things that are not the problem:
Things that we haven't checked:
I recommend that the first thing in the morning operators take the ISC lock guardian to locking arms green, wait there for 10-20 minutes, and look at second trends of the arm transmissions. You can compare them to the screenshot I've attached here, if the glitches are gone or much smaller it would be worth doing an initial alignment and trying to lock to DC readout, if the glitches are still there it is not worth trying.
A surprising number of the small glitches in Y align with bigger glitches in X. We should take a look at the fiber distribution.
zooming in you really can see that some of them are aligned.
Fibers including ALS fiber with flapping tag. The fan of the network equipment is blowing directly on it.
Daniel pinged this and both arms unlocked. It's not clear this is the problem but it's not good anyway and will be fixed. (WP7015)
Richard's solution was a yellow tubing around the fibers. A stuffed bag as a wind barrier is probably Daniel's thing.
After that the glitches seem to have been gone. We'll see if ALS survives longer than 10 minutes.
perhaps we can put the side panel on the networking rack. I suspect we left it off since the Cisco core switch is sideways venting.
CP3 log file DOES NOT exist! CP4 Fill completed in 258 seconds. Starting CP4 fill. LLCV enabled. LLCV set to manual control. LLCV set to 70% open. Fill completed in 258 seconds. TC A did not register fill. LLCV set back to 41.0% open.
1. When I came in, Y VCO "tune ofst" was railing at -5V ("tune mon" 8.3V or so). As such, the VCO frequency was higher than 80 MHz (set frequency is 78.92MHz) and the beat note somewhat above 40MHz. Manually resetting it, "frequency servo" brought it back. This is will PLL only, no PDH. I thought that the "tune mon" is the readback of the VCO "tune" input on the front panel, but it was 8.3V even when I terminated the BNC. Apparently I forgot these things.
2. At the end station, I reseated the two slow controls cables for PDH CM board at Beckhoff chassis end, and locked the arm green, no change in glitches.
3. Connected the CM tester to refl CM to lock the arm but failed. I think the tester setting was good but maybe some automation was doing something funny though I disabled the state machine in the ALS overview. Refl CM was put back on slow controls cables.
4. Switched the PFD channel, locked the arm, glitches persist. Switched it back.
5. Time's up for the day.
Keita arrived in the control and noticed vacuum alarms relating to the Vacuum gauge at CP2, PT134B, and the Corner Station instrument air ??199. PT134B is currently off and shows up as "RED" MEDM field on the vacuum screens. This has been discussed in entries made previously and is being pursued by Gerardo M., Chandra R. and Richard M.. The instrument air alarm may be a stale alarm from when before Bubba replaced the GV8 instrument air supply pressure regulator. If so, it could be acknowledged and should not re-occur. There still may be a "low pressure" condition which would result in a new instrument air alarm. Control room folks - 1. Ignore PT134B alarm, 2. Acknowledge ??199 instrument air alarm and treat new occurrences of this alarm as valid. We are monitoring remotely periodically.
done and done
Remote logged in to toggle PT-134, CC was off when I logged in.
I turned on and off the CC several time to try to get it to get on scale, but no luck. Left the CC on, but it is not on scale, sometimes they take long to do so.
https://services.ligo-la.caltech.edu/FRS/show_bug.cgi?id=8265
CP3 log file DOES NOT exist! CP4 Fill completed in 298 seconds. Starting CP4 fill. LLCV enabled. LLCV set to manual control. LLCV set to 70% open. Fill completed in 298 seconds. TC A did not register fill. LLCV set back to 41.0% open.
Bubba, Kyle Fixing Corner Station instrument air. LVEA and chiller yard. Will make comment to this entry when leaving site.
The o-ring on the same regulator that was repaired yesterday blew out again. This time I replaced the entire regulator, slightly different style but no leaks on this one. I believe the old regulator had just worn out. GV 7 & 8 gate cylinders are back under normal supply air pressure and open.
1255 hrs. local -> Leaving site now.
here is a minute trend (mean) plot of CP3's pump level and LLCV position over the past 24 hours showing good control of the LN2 level at the 92% set point. Reminder that only CP4 will autofill in 20 minutes time.
TITLE: 06/03 Eve Shift: 23:00-07:00 UTC (16:00-00:00 PST), all times posted in UTC
STATE of H1: Planned Engineering
INCOMING OPERATOR: None
SHIFT SUMMARY: I tried to lock ALS a few times after commissioners left to no success. Y would complain of VCO problems and would not hold the a lock longer than a few tens of seconds. No one relieving me, and no day operator tomorrow.
LOG:
1925 hrs. local I found the rotometer ball off of the stop about 1/2 the diameter of the ball (< 0.4 LPM the smallest graduation of the flow scale). When the isolation valve at the plumbing manifold was closed, this small flow stopped, i.e. the ball rested. This was repeatable. This could be flow across the sensing line blockage or it could also be leakage flow out of the 4 or 5 pipe joints which can't be isolated. Anyway, this wasn't occurring the last time I inspected it. The UHP N2 bottle is at 1800 psi tonight, down 300 psi from 24 hrs. ago. While there, I repeated the exercise of switching between pumping the sensing line with a small vacuum pump then switching to pressurizing with the UHP N2. I had made a few attempts at this yesterday? the day before? but could never establish any flow. Tonight, I was able to achieve flow for 10s of seconds at a time. I would have like to have continued this as it is so encouraging but I don't want my children to grow up without knowing their daddy + plus I'm hungry plus ..... I am leaving the apparatus at 60 psi regulator output and adjusted for 2 LPM max.
Fil, Daniel, Jenne, Keita, Patrick, Richard, Sheila, Kiwamu,
The investigation continues. No solid conclusion or resolution yet.
Just to summarize what we think we know so far:
Things that were exonerated by bypassing PLL test:
Other things that we think are exonerated:
Things that we haven't eliminated:
TITLE: 06/02 Eve Shift: 23:00-07:00 UTC (16:00-00:00 PST), all times posted in UTC
STATE of H1: Planned Engineering
OUTGOING OPERATOR: Ed
CURRENT ENVIRONMENT:
Wind: 7mph Gusts, 4mph 5min avg
Primary useism: 3.58 μm/s
Secondary useism: 0.87 μm/s
QUICK SUMMARY: ALS work continues. 6.9M earthquake off of Alaska will be hindering us for a bit.
TITLE: 06/02 Day Shift: 15:00-23:00 UTC (08:00-16:00 PST), all times posted in UTC
STATE of H1: Planned Engineering
INCOMING OPERATOR: TJ
SHIFT SUMMARY:
LOG:
15:00 Sheila to EY to investigate ALSY PLL.
15:15 sensor correction turned of at EY
15:46 Jim doing TFs on HAM5
16:00 Sheila back
16:05 SC turned back on at EY
16:11 Granted Aiden remote access
16:14 Richard transitioning LVEA to LASER SAFE
16:31 SC back OFF on EY - Kiwamu heading back out
16:54 Betsy in LVEA to look through TCS cabinets
16:57 Ken into LVEA to look for a ladder
17:07 Ken out
17:10 Richard and Kiwamu restarting ISC EY computers
17:21 Betsy out. Heading to the MX in 15 minutes.
17:38 Richard back from EY
17:58 Bubba into the LVEA
18:38 Kiwamu back
18:44 Gerardo going into LVEA
18:54 Gerardo out
19:18 Fil going to EY to switch out a common mode servo chassis for ALS
20:02 Fil back
20:46 Fil goin back to end station. Newly installed chassis not responding
20:46 Peter into the optics lab
22:00 Crew back at EY working on ALS
22:30 6.9mag EQ in Alaska 30um/s
The faulty regulator which turned out to be only a bad o-ring in the regulator itself, has been repaired, reinstalled, and air is flowing again. I unlocked the valves with Chandra watching the vacuum screen in the control room. While I was repairing the regulator, Kyle was ordering a couple of new regulators for spares. Chandra and I also replaced the check valves on the corner station instrument air compressor.
The regulator failed again the next day, so we replaced it with an odd ball spare. Awaiting order delivery of direct replacements.
CP3's reservoir level is back on scale - reading around 97% full. I lowered the PID lower limit of LLCV to 15% open when it was ~99% full to measure percentage per hour to get a feel for how low the reservoir got over the weekend.
PID is programmed to hold the reservoir at 92% full. Once it drops to that level, PI will kick in.
This proves LIGO is not a hoax. Nobody could make this story up.
A story worth documenting! Can we warm up CP4 next? ;)
PI performance looks good. And there is no smoothing factor set. At 15% open on LLCV, rate of decline is 2.3% per hour given today's temperatures.