Displaying reports 65741-65760 of 83394.Go to page Start 3284 3285 3286 3287 3288 3289 3290 3291 3292 End
Reports until 02:32, Friday 01 May 2015
H1 ISC
kiwamu.izumi@LIGO.ORG - posted 02:32, Friday 01 May 2015 (18131)
locking rehabilitation, back to high recycling gain, low noise ETMY and OMC

Jeff K, Kiwamu, Jim W,

As a prep for the mini run, we aimed to confirm that we can run in the low noise state. Most of the attemps were successful today and the interferometer stayed at a recycling gain of more than 35 most of the time and 39 at one point.

Here are items that we could not get done today:

Also, an earth quake hit us at around 8:20 UTC which we think is from Papua New Guinea at around 8:06 UTC with 7.1 M. This is a good execuse to go home for the night.

 

(ITM camera position updated)

As planned yesterday (alog 18125), we did initial alignment from scrach. We started from the classic dither-based TMS alignment which gave us well-centered beam on ITMs. Then ITMs and ETMs were manually aligned to obtain high build up in the arm cavities for the green light. After this arm alignment, we updated the ITM camera positions. Moreover, we did the Y arm red/green co-alignment again. We started from BS alignment using the ETMY baffle (see for example alog 18035) and optimized ITMY and ETMY to get high build up in red. Then steered TMSY and green QPD pointing to maximize the green transmitted light. I introduced offsets of -0.2 and 0.2 counts in QPD_A_YAW and QPD_B_YAW respectively. Note that these QPD offsets were confirmed to be good afterwords with the interferometer fully locked and optimized for high recycling gain.

The full-scratch alignment seemed to have helped increasing the recycling gain and therefore we did not have an issue in reducing the CARM offset which was very problematic yesterday seemingly due to a poor recycling gain (alog 18125). Once we fully locked the interferometer, we maximized the recycling gain by manually steering both ITMs in pitch and yaw as usual. This resulted in a recycling gain of 39 acrroding to TRX and TRY. The camera positions were then updated again for the high recycling gain condition. Also, I updated the ITMY aperture which I disabled two days ago (alog 18108) because the aperture was basically not doing a good job at all. I attach a picture of the ITMY camera with the new aperture masking. This seems to be working fine so far.

 

(Some udpates on ISC_LOCK guardian)

Since we have been focusing on the recycling gain issue in the past days, many commands (e.g. ASC roll offs (alog 17966) and etc.) had been commented out in ISC_LOCK which had helped the interferometer staying robust. However for the automation purpose for mini run, I uncommented all the commented lines in ENGAGE ASC so that now it engages all the loops. So far we did not see an issue with these ASC loops except for the DHARD/CHARD roll offs which apparently make the loops unstable for some reason. They remain uncommented. Also, I kept the roll mode damping commands commented out because I am worried about a situation where the modes rang up so high that the damping signals saturate the DACs. We increased the DARM offset from 2x10-5 to 3x10-5 counts in order to obtain more light on the OMC DCPDs. This gave us a total current of 10 mA when PSL was at 2.7 W.

After we edited the guardian, we confirmed that the ISC_LOCK could take us up to the low noise ETMY ESD state. This is a step far from the final state, the LSC feedforward. We did not get a chance to check out the LSC feed forward tonight.

Images attached to this report
H1 ISC
daniel.hoak@LIGO.ORG - posted 23:31, Thursday 30 April 2015 (18130)
OMC work: length dither frequency, loop shaping, alignment dither is working again

After we got back to low noise (yay!), I spent a few hours working on the OMC.  The salient points are:

 

OMC Length Dither Frequency

Koji recommended that the dither frequency be changed to move away from some excess noise he suspected was polluting the error signal.  I scanned the dither frequency from 3300Hz to 4900Hz in 200Hz steps.  Sure enough, there is a bump of excess noise around 3335Hz that had been coupling to the length error signal when the frequency was set to 3300Hz.

The first plot attached shows the sidebands and excess noise structure for these different frequencies (the channel plotted is the OMC-DCPD RIN).  It's not a very convincing plot, but setting the frequency at 4100Hz gave us the cleanest spectrum.  (I will post more convincing measurements later.)  It would be good to do a finer scan in the future.  I think the dither frequency at L1 is currently 4800Hz.

As the dither frequency was scanned I monitored an excitation at 12Hz into PZT2, this was necessary to keep track of which quadrature of the demodulated dither signal was the best measure of the length of the cavity.  Here's the data keeping track of how the length excitation rotated from COS to SIN as the dither frequency was changed:

Dither Frequency COS/EXC (mag, dB) COS/EXC (phase, deg) SIN/EXC (mag, dB) SIN/EXC (phase, deg) Demod Phase to lock the servo
3300 -27 65 -27 -110 90
3500 -26 85 -61 -40 90
3700 -27 65 -27 65 90
3900 -35 37 -25 37 90
4100 -35 -105 -25 80 0
4300 -26 -125 -28 55 0
4500 -25 -95 -50 no coherence -90
4700 -25 -105 -25 -100 -90
4900 -50 no coherence -25 -70 180

Since the phase was changing it was necessary to adjust the demod phase to put the right quadrature into the length loop.  (Why is the phase changing?  Is it from a digital delay, or a mechanical resonance in the PZT?)

 

 

OMC Length Loop Shape

With the dither frequency set I inserted a 200Hz-wide bandpass around the dither frequency before the demodulation, and removed all of the ELPs and butterworth LPs that we had been using to suppress demodulated junk from getting into the control signal.  An OLTF is attached (Fig 2), the UGF is 10Hz -- still a little high, from Koji's measurement -- and there is 67deg of phase margin.  (In the legend, the green trace is the demod input highpassed, not lowpassed.)

The correct filters to use in the OMC length loop path are now:

LSC-PD_IN: FM2,5 (butterfly bandstop, 200Hz bandpass around 4100Hz)

LSC-X_COS, LSC-X_SIN: FM2 (double ELP for notch at 4100Hz)

LSC-SERVO: FM1, 2, 6, 8, 10 (boost, integrator, anti-dewhites and calibration constants)

This will give you a loop that looks like the blue trace in Fig 2.  The gain of the servo is still set to 10.

 

OMC Alignment Dither

We've changed the alignment dither frequencies to [1675.1, 1700.1, 1725.1, 1750.1] Hz, but we never re-commissioned the loops.  Today I spent quite a while trying to measure a dither sensing matrix with excitations into the QPD loops at 1.1Hz.  This never produced an answer that worked upon inverting.  Kiwamu mentions that things might be complicated by the actuation on the OMC SUS, and AC excitations could be exciting other DOFs than what we want to measure.

In the end I measured a sensing matrix at DC, with offsets into the QPD loops, inverted and got something that worked.  We can engage the dither loops now, but I recommend ramping down the QPD loops (with the master gain slider), switching to the dither input, and then turning up the gain.  It's probably good to keep the gain low, at 0.4, this gives a response to DC offsets of ~10 seconds.  I didn't have a chance to measure the sensing noise to estimate the useful bandwidth. This has not been added to the OMC Guardian.

Images attached to this report
LHO General
john.worden@LIGO.ORG - posted 10:24, Thursday 30 April 2015 (18127)
3IFO storage vessels

Attached are the dewpoint sensors for the 14 monitored storage containers. All data is shown since the sensors were installed and cabled.

Images attached to this report
H1 ISC
kiwamu.izumi@LIGO.ORG - posted 03:33, Thursday 30 April 2015 (18125)
locking attempt with no success tonight

Dan, Kiwamu,

We had trouble locking the interferometer tonight and therefore did not reach full lock.

It seems that the recycling gain is very low for some reason tonight. It seems as low as 19. Therefore the CARM reduction did not work as intended. In fact, REFL_LF dropped below 40% or less even when we were at the CARM_15PM state. Every time when we moved onto CARM_10PM it lead to lock loss. Not good. We even tried to transition to TR_REFL mutilple times by skipping a few CARM reduction steps since the REFL9 seemed passing the turn-around point. However this did not work either. Sad.

We co-aligned both red and green light in the Y arm in order to improve the recycling gain, but this did not seem to help. I am thinking of starting from the baffle PDs tomorrow in both arms just to make sure alignment is reasonable. In the course of the Y arm alignment tonight, we had to realign the ALS diff beatnote once because it went lower than -10 dBm.

PRC2 ASC loop still does not work only in yaw as reported by Dan (alog 18109).

H1 SUS
kiwamu.izumi@LIGO.ORG - posted 01:37, Thursday 30 April 2015 (18124)
ETMX ESD wiring fixed

There was a cabling error for the ETMX ESD DAC signals and this was the reason why we could not untrip the ESD driver. This is now fixed.

I drove down to EX and investigated the issue and found out that calbe #85 (see D1992741-v8) was conected to a wrong input of the AI chasis (S1102380). This must have been introduced today during the AA/AI chasis activity (see alog 18117). Since Stuart's medm screen (alog 17585) relies on the ability to see the analog signals, it was not able to tell whether the ESD driver was on or off even though the binary switches have been functional. I connected the cable back to the correct position which is the first slot (ch1-4) from the left on the front panel of the AI chasis. This fixed the issue -- now we can untrip and drive the ESD.

H1 PSL
kiwamu.izumi@LIGO.ORG - posted 00:58, Thursday 30 April 2015 (18123)
PSL tripped at around 22:30 UTC, restarted

Seemingly due to some flow sensor issues. I reset the flow sensor indicator back to green in the control room. Then I reset the interlock and restarted the frontend from the diode room.

H1 TCS (TCS)
greg.grabeel@LIGO.ORG - posted 18:23, Wednesday 29 April 2015 (18122)
HWS rough alignment
Nutsinee, Greg
Alignment continued in two parts today. We first aligned the SLED beams to the irises on the table while waiting for a green beam to return. Once we got a green beam we attempted to align the SLEDs to the green beam. The Y side looks like it could use some continued refinement, while the X side continued to give us fits until the commissioner asked to give him back the interferometer. 
Images attached to this report
LHO VE
kyle.ryan@LIGO.ORG - posted 17:20, Wednesday 29 April 2015 - last comment - 11:05, Thursday 30 April 2015(18121)
1030 - 1530 hrs. local -> Leak checking at X-end
Kyle, Gerardo 

Today we wanted to quantify the gas load "contribution" of the known leaking all-metal 2.5" Vent/Purge valve at the X-end station.  

SETUP 
X-end open to BT (GV19, GV20 open)
Main Turbo backed only by the leak detector (no parallel pumping)
 

RESULTS 
LD helium baseline < 10-10 torr*L/sec before valving turbo into X-end volume
Helium background signal = 3 x 10-8 torr*L/sec after valving turbo into X-end volume 
Valved-out IP12 
Removed NW50 blank from closed Vent/Purge 2.5" all-metal valve (i.e. vented air side of closed metal valve) 
X-end pressure responded by rising to low 10-7 torr 
Sprayed audible flow of helium on air side of closed valve while monitoring helium signal 
Helium signal rose rapidly then leveled-off and peaked at 2 x 10-5 torr*L/sec (signal peaked after ~10 seconds of spraying but I continued spraying until ~30 seconds) 
Spent the next few hours pumping system with the turbo pump to remove introduced helium.  We also added an O-ring valve in series with the leaking valve and evacuated the air side of this valve 

CONCLUSION 
Traditionally we have only used the vendor supplied hand knobs to open/close these Vent/Purge 2.5" metal valves (1 per isolate-able volume).  The allowable torque specs far exceed what can be applied using these knobs.  As such, our valves are likely under-torqued as a rule and, as was demonstrated yesterday, this leak could likely be eliminated by tighing this valve using a wrench.  As this particular valve has a "gappy" conflat joint on the vacuum side, we didn't want to "fix" it using a wrench (long lever) while we are open to the BT and while commissioning time is at a premium.  The main take away is that all of our poor pressure level at the X-end can be attributed to this under-torqued metal valve and that we have no reason to suspect GV19 or GV20.
Comments related to this report
kyle.ryan@LIGO.ORG - 11:05, Thursday 30 April 2015 (18128)
Helium level in vacuum system was 3 x 10-8 torr*l/sec before testing (spraying), peaked at 2 x 10-5 torr*L/sec during testing and was 5 x 10-8 torr*L/sec after 3 hours of pumping with turbo following completion of testing.
H1 INJ (CAL)
jeffrey.kissel@LIGO.ORG - posted 16:25, Wednesday 29 April 2015 (18120)
H1 INJ Path Tested with awggui
J. Kissel, M. Landry

We've confirmed that hardware injection signals can go from each hardware excitation point that will be accessed by the non-blind and blind hardware injection team all the way out to the ETM SUS. We've done so with a 1 [Hz] sine wave awggui excitation from each of the injection filter banks. It turns out awggui can't request a gain of less than 1e-6, so each of our excitations which passed through the new inverse actuation filter (LHO aLOG 18115) were, shall we say... ridiculously large. But, at least it passed the signal chain test.

We'll work on getting unit-full text files of physical waveforms from the search groups (that are of amplitudes ~1e-21 or 1e-22 in strain instead of 1e-6) tomorrow. 
H1 General
travis.sadecki@LIGO.ORG - posted 16:02, Wednesday 29 April 2015 (18117)
OPS Day Shift Summary

7:00-8:00 Cris and Karen in LVEA

8:17 Fil and Ed to EX AA/AI work

8:21 Richard and TJ to EY AA/AI work

8:52 Karen to MY

9:37 Kyle and Gerardo to EX

9:49 Karen done at MY

10:35 Fil and Ed done

10:39 Kyle and Gerardo to LVEA, then EX

12:00 Greg and Nutsinee to LVEA

13:13 Greg and Nutsinee done

15:52 Kyle and Gerardo done

H1 SEI
thomas.shaffer@LIGO.ORG - posted 15:33, Wednesday 29 April 2015 (18119)
BRS Damper Turned OFF and masses adjusted

Due to high traffic in the X end today, the BRS was rung up pretty high. SYS_DIAG showed the BRS rung up as well as the damper out of range. Jim w. and I decided that it would be best for it to settle with the damper off. So, I went to EX and turned the BRS Damper OFF and will leave it commented out until it settles down.  When I went to go inspect the masses I found that they were about 45 degrees off, aligned with the tube, so I moved them back to their North-East and South-West positions.

H1 General
travis.sadecki@LIGO.ORG - posted 14:41, Wednesday 29 April 2015 (18118)
Morning meeting notes

SEI running TFs on ITMy, BS, and ETMx ISIs

AA/AI work at both end stations

RGA work at EY

Leak checking ongoing at EX

H1 INJ (CAL, DetChar, INJ, ISC)
jeffrey.kissel@LIGO.ORG - posted 14:37, Wednesday 29 April 2015 (18115)
First Cut at H1 Hardware Injection Calibration Filters Installed
J. Kissel

I've installed the first cut of the inverse actuation filter for the hardware injection team, based on the model shown in LHO aLOG 18050, but originally described in detail, with uncertainties in LHO aLOG 17951 and LHO aLOG 18039. Exactly the same filters have been installed in both the HARDWARE and BLND filter banks.

Design Details:
%%%%%%%%%%%%%%
I've divided the filter into two banks: 
- FM1 "Inv.Act" = the "main" [ct/m] inverse actuation function described below, and 
- FM10 "m_per_strain" = a gain-only filter that is equivalent to the mean IFO arm length of mean([3994.4704 3994.4692]) =  3994.47 [m]

For the "main" [ct/m] inverse actuation function I
- saw that the model parameters of the past six actuation functions we've reconstructed show results that are virtually identical above 20 [Hz], (see pg 1 of attached .pdf)
- grabbed the latest one of these actuation function models from Apr 15 2015 (parameters from H1DARMparams_1113119652.m),
- inverted it, and
- compared/"fit" it against a simple zpk filter that I knew I could easily hand-implement in foton (see pg 2 of the attached .pdf)

I ended up with the following filter:
Matlab Notation:
    toyModel.poles_Hz = [pair(4e3,51) 6e3];
    toyModel.zeros_Hz = [0.01 0.01];
    toyModel.gain     = 5.98e9;
Foton Design String:
    zpk([0.01;0.01],[2517.28+i*3108.58;2517.28-i*3108.58;6000],1,"n")gain(9.51664e+08)
where the gain has been normalized to match the real model at ~100 [Hz] in matlab, and forced to match the matlab at 99.54 [Hz] in foton (see gain forcing in 2015-04-29_H1DARMINJ_FotonDesign_and_MEDM.png). 
Bode plots of these filters implemented in foton can be found in the last two pages of the attached .pdf.

HOWEVER
You'll notice that the "real" model of the inverse actuation function (a) goes to infinity at high frequency, and (b) has phase behavior equivalent to that of a time *advance*. As such, I've made the following design choices / approximations with this simple model of the inverse actuation:
- Without the ability to make higher-than-Nyquist frequency poles, or to have a filter with more zeros than poles, I've rolled off the function at ~5 [kHz] with the above design (note the pair of poles with some complex phase in between is to tweak up the magnitude to achieve good fidelity reproduction out to 2 [kHz]).
- Of course, we must also, unfortunately have *casual* filters in the front end. As such, I compute the amount of time *advance* we need to reconstruct the phase response reasonably well. This is ~250 [us]. or 4.1 16384 [Hz] cycles.

I'M HOPING that the hardware injection team has this ability, to merely time-shift or "mis"-time-stamp their injection at the sub-millisecond time precision, or some how program the injection to happen 4 clock cycles "in the future." We'll be discussing this on the HW INJ call tomorrow to be sure.

Comments on Accuracy and Precision
%%%%%%%%%%%%%%%%%%%%%%%%%%%%%%%%%%
Recall from LHO aLOG 18039, that we are confident in the frequency dependence of the open loop gain to +/- 2.5% in magnitude and 1 [deg] between 15 and 700 [Hz] (and probably out to several [kHz], we just don't have any measurements to that high a frequency yet). However, the uncertainty in the overall scale factor is still ~26% (because we haven't yet discerned the scale factor uncertainty between optical gain fluctuations of the sensing function and ESD actuation strength varying due to charge fluctuations).

As such, I would assign the same uncertainty to the inverse actuation function alone, in addition to the residuals between the real model and this simple fit to it. These residuals are less than 1% and 0.5 [deg] between 15 - 1500 [Hz]. In summary, the 1-sigma, 68% confidence intervals are
Overall Scale: 26%, Frequency Dependence: 2.7%, 1 [deg] between 15 and 700 [Hz] (but likely out to 2 [kHz])
Images attached to this report
Non-image files attached to this report
H1 SUS (SEI, SUS)
richard.mccarthy@LIGO.ORG - posted 14:23, Wednesday 29 April 2015 (18116)
SEI SUS AA/AI boards replaced
Per Work permit 5173

A continuation of the work done yesterday.  Today the Seismic and Suspension AA/AI chassis at bot EX and EY were swapped for V6 chassis.  All Chassis in the electronics room have been addressed at this time and are V6.

LHO VE
john.worden@LIGO.ORG - posted 12:08, Wednesday 29 April 2015 (18114)
Leak checking underway at XEND

The pressure at XEND has stepped up to 1e-7 due to the leak testing activity. No cause for alarm as this appears to be the purge valve leaking. More info to come later today.

H1 SEI
hugh.radkins@LIGO.ORG - posted 10:14, Wednesday 29 April 2015 (18113)
LHO SEI STS2-B Study Update

Here are plots from yesterday, again around 0130pdt like previous posts: Monday, Friday (18046), and Wednesday (18007.)

Again (looking at the ASDs,) the Z channel looks like all the others and better for STS2-B (ITMY) compared to reference (old seismo.)  Also, the X axes all look good (similar) now (compared to Monday.)  Before it wasn't clear, maybe the seismic environment wasn't as benign as I thought.  For the Y DOF ASDs, HAM5 & ITMY sensors diverge below 20mHz but more telling, the HAM2 Y DOF goes off track from the other two around 70 or 80 mHz.  The traces also look differnt relative to the Noise trace, something has happened to the calibration I need to sus out.

The TFs I've presented before are a little too busy.  I'll rework their arrangement for the future.

Images attached to this report
H1 CDS
patrick.thomas@LIGO.ORG - posted 09:06, Wednesday 29 April 2015 (18112)
Updated Conlog channel list
Added 804 channels. Removed 918 channels.

2 channels remain unmonitored:
H1:SUS-SR2_LKIN_P_OSC_SW2R
H1:SUS-SR2_LKIN_Y_OSC_SW2R
LHO VE
bubba.gateley@LIGO.ORG - posted 09:02, Wednesday 29 April 2015 (18111)
Beam Tube Washing
Scott L. Ed P. Chris S. 

4/27/15 the crew worked on crevice and tube cleaning ending 2.3 meters north of HNW-4-016. Tested clean areas (posted on this report) and began moving lights and cords to the next section. Vacuumed support tubes and sprayed bleach/water solution.

4/28/15 continued vacuuming and began tube cleaning. Cleaned 55 meters ending 17.5 meters north of HNW-4-018.
Non-image files attached to this report
H1 ISC
evan.hall@LIGO.ORG - posted 05:00, Thursday 16 April 2015 - last comment - 06:12, Thursday 30 April 2015(17905)
FF performance: MICH ok, SRCL not good

Koji, Evan

Summary

MICH feedforward seems to be doing its job, although there is room for improvement by implementing a frequency-dependent subtraction.

SRCL coupling into DARM seems to be very nonstationary. Consequently, the feedforward is not working.

Details

We injected band-limited white noise (elliptic bandpass, 10 Hz to 1 kHz, 6 ct amplitude) first into MICH, then into SRCL, to test the feedforward that was implemented a few weeks ago.

For MICH, frequency-independent subtraction is fair to middling (red) compared to no subtraction (blue); at best we get 20 dB of subtraction around 150 Hz. Note that the TFs in this plot use the whitened DARM channel. The whitening is undone for the spectra in the fourth pad.

For SRCL, the 1/f2 feedforward via ITMY L2 gives no subtraction at all. The attachment shows the TF of SRCL control → DARM with the feedforward off and with broadband noise injected into the SRCL error point. Unlike MICH, appearance of this excitation in DARM is highly nonstationary, fluctuating by a factor of 2 or so in a frequency-dependent way. Additionally, the coherence is poor above 20 Hz, despite the excitation elevating the DARM noise by more than an order of magnitude from 20 to 100 Hz.

The shape of the excess noise is more or less the shape of the 100 Hz elliptic cutoff that we put into SRCL a few weeks ago. Is it possible that the SRCL control noise explains the nonstationary, 100 Hz "scattering" shelf that we've seen in the DARM spectrum this past week?

Images attached to this report
Comments related to this report
evan.hall@LIGO.ORG - 07:59, Thursday 16 April 2015 (17907)

Using the measurements described above, here is a projection of MICH and SRCL control into DARM. It seems that these two noise sources, along with DAC→ESD noise, can explain most of the DARM noise from 10 to 70 Hz. There is still some excess from 80 to 200 Hz, and an overall excess in the high-frequency noise floor.

For MICH, I used the coherent transfer function we measured earlier. For SRCL, I estimated the TF magnitude by dividing the ASDs of DARM and SRCL (after subtracting off their quiescent values). The dtt files are in evan.hall/Public/2015/04/FullIFO/Noise as MichNoise.xml and SrclNoise.xml.

Some times (all UTC):

  • Quiet data: 07:55:00 to 08:02:00
  • MICH excitation: 08:12:22 to 08:14:22 with MICH FF off, 08:08:58 to 08:10:58 with MICH FF on
  • SRCL excitation: 09:22:10 to 09:25:10 with MICH FF and SRCL FF on, 09:26:05 to 09:28:05 with MICH FF on and SRCL FF off, and 09:28:15 to 09:30:15, no FF.

After these measurements, I also tuned the PRCL→SRCL subtraction in the LSC input matrix from 0.005 to -0.04 (using in-vac POP). This reduced the appearance of a 122 Hz PRCL excitation in the SRCL error signal by 20 dB.

Non-image files attached to this comment
evan.hall@LIGO.ORG - 22:32, Sunday 19 April 2015 (17947)

For completeness, here is the same budget as above, with intensity and frequency noises included.

We suspect that the sharp shelf at 100 Hz in the frequency noise projection might be coupling via SRCL, rather than directly to DARM. So between the frequency and SRCL projections, there may be some double-counting of noise in DARM.

Frequency, intensity, and DCPD dark noise are not enough to explain the excess noise between 200 Hz and 4 kHz. It seems they can somewhat explain the uptick in noise above 4 kHz.

Non-image files attached to this comment
evan.hall@LIGO.ORG - 06:12, Thursday 30 April 2015 (18126)

Slightly updated/corrected version attached.

Non-image files attached to this comment
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