[Alexa, Kiwamu, Koji]
We found that IMC WFS B had quite small error signals. We tracked down this to be too small LO.
What we found was the LO cable had bad connection at the SMA connector. This is the same problem as Kiwamu reported before.
After recrimping the IMC WFS B cable, the all of the cables on ISC-R2 rack was reviewed.
All of the cables had the same crimping issue. Also, most of the SMA were not secured.
All of the SMA cables were recrimped and 4~5 SMAs have been replaced.
Here is the list of the LO powers in the monitor. WFS REFL45 has CH1 and CH2 with +13dBm LO power
while CH3/4 indicates very low numbers. In fact these nubers (and the corresponding RF power mons)
are not changing at all. So this could be a DAQ related problem.
=== Rack ISC-R1 U07 ===
H1:IMC-WFS_A_DEMOD_LOMONCHANNEL_1 = 16.0804
H1:IMC-WFS_A_DEMOD_LOMONCHANNEL_2 = 15.9532
H1:IMC-WFS_A_DEMOD_LOMONCHANNEL_3 = 15.999
H1:IMC-WFS_A_DEMOD_LOMONCHANNEL_4 = 16.5534
=== Rack ISC-R1 U05 ===
H1:IMC-WFS_B_DEMOD_LOMONCHANNEL_1 = 16.1007
H1:IMC-WFS_B_DEMOD_LOMONCHANNEL_2 = 16.1821
H1:IMC-WFS_B_DEMOD_LOMONCHANNEL_3 = 16.1618
H1:IMC-WFS_B_DEMOD_LOMONCHANNEL_4 = 16.3296
=== Rack ISC-R2 U38 ===
H1:ISC-RF_C_REFLAMP45M_OUTPUTMON = 17.5009
=== Rack ISC-R2 U37 ===
H1:ISC-RF_C_REFLAMP9M1_OUTPUTMON = 20.2811
=== Rack ISC-R2 U34 ===
H1:LSC-REFLAIR_A_RF9_DEMOD_LOMON = 20.6277
H1:LSC-REFL_A_RF9_DEMOD_LOMON = 20.9278
=== Rack ISC-R2 U30 ===
H1:LSC-POPAIR_A_RF9_DEMOD_LOMON = 23.059
H1:LSC-POPAIR_A_RF45_DEMOD_LOMON = 19.8342
H1:LSC-REFLAIR_A_RF9_DEMOD_LOMON = 20.6073
H1:LSC-REFLAIR_A_RF45_DEMOD_LOMON = 19.8494
=== Rack ISC-R2 U28 ===
H1:LSC-POPAIR_B_RF18_DEMOD_LOMON = 22.5656
H1:LSC-POPAIR_B_RF90_DEMOD_LOMON = 20.1851
H1:LSC-REFLAIR_B_RF27_DEMOD_LOMON = 23.0234
H1:LSC-REFLAIR_B_RF135_DEMOD_LOMON = 18.0488
=== Rack ISC-R2 U24 ===
H1:LSC-POP_A_RF9_DEMOD_LOMON = 23.3642
H1:LSC-POP_A_RF45_DEMOD_LOMON = 19.8494
H1:LSC-REFL_A_RF9_DEMOD_LOMON = 20.9328
H1:LSC-REFL_A_RF45_DEMOD_LOMON = 20.119
=== Rack ISC-R2 U18 ===
H1:ASC-REFL_A_RF9_DEMOD_LOMONCHANNEL_1 = 17.174
H1:ASC-REFL_A_RF9_DEMOD_LOMONCHANNEL_2 = 17.0824
H1:ASC-REFL_A_RF9_DEMOD_LOMONCHANNEL_3 = 16.94
H1:ASC-REFL_A_RF9_DEMOD_LOMONCHANNEL_4 = 17.3011
=== Rack ISC-R2 U16 ===
H1:ASC-REFL_A_RF45_DEMOD_LOMONCHANNEL_1 = 13.3693
H1:ASC-REFL_A_RF45_DEMOD_LOMONCHANNEL_2 = 13.471
H1:ASC-REFL_A_RF45_DEMOD_LOMONCHANNEL_3 = -75.0432
H1:ASC-REFL_A_RF45_DEMOD_LOMONCHANNEL_4 = -74.9568
=== Rack ISC-R2 U10 ===
H1:ASC-REFL_B_RF9_DEMOD_LOMONCHANNEL_1 = 17.3215
H1:ASC-REFL_B_RF9_DEMOD_LOMONCHANNEL_2 = 17.2604
H1:ASC-REFL_B_RF9_DEMOD_LOMONCHANNEL_3 = 17.2096
H1:ASC-REFL_B_RF9_DEMOD_LOMONCHANNEL_4 = 17.3011
=== Rack ISC-R2 U08 ===
H1:ASC-REFL_B_RF45_DEMOD_LOMONCHANNEL_1 = 13.5117
H1:ASC-REFL_B_RF45_DEMOD_LOMONCHANNEL_2 = 13.1913
H1:ASC-REFL_B_RF45_DEMOD_LOMONCHANNEL_3 = 13.3642
H1:ASC-REFL_B_RF45_DEMOD_LOMONCHANNEL_4 = 13.4558
BSC9 annulus not pumping yet -> Problem with aux. pump cart
Gerardo already pumping BSC1 and HAM3 -> will continues leak hunting on Monday
There seems to be some slow oscillating taking the outputs to higher values (1000+.) unlike the ITMX, it doesn't seem to go out of control bt the larger values are still worrysome to me.
I'll move it to isolated damped for the weekend.
Took a couple of photos of ETMY after Rai's discharging work was completed. As with yesterday's pictures, it's tough to tell if there's any dust on the surfaces or not. Tried focus stacking for image ETMY2.jpg in order to improve the depth of field. Didn't seem any better than simply shooting with a smaller aperture. All images are quite large, so there's no preview available. RichardM, PeterK
I may not get to fixing this tonight so I at least wanted to report it.
I think Stage1 Isolation is ok but when Stage2 is Isolated, it looks like it rings up exciting stage1 and both tripping on Actuators. HEPI is not tripping.
Currently, ITMX is under managed guardian at Isolated_Damped.
12:15 Fred et al out of LVEA 13:00 Doug, Jason done at ITMY 13:15 Gerardo to LVEA looking for pump cart, pump HAM4 annulus 13:30 Karen to EY 13:30 RichardM to EY to verify an interlock is working, back to 14:30 14:00 GregG turning on CO2 laser in squeezer bay 14:15 Fil, Manny to EX for ISC WFS cabling 15:00 Jason to BS oplev, done 15:15 16:00 Pablo to EX to work on VCO characterization
Start time 11:00 am.
Pressure as of 1:46 pm 2.0 x 10-5 torr at the aux cart.
Start time was 10:30 am.
Current pressure as of 1:45 pm 1.3 x 10-5 torr.
Morning Shift Notes 916 - Nathan beginning work in the OSB laser lab 920 - Rai to EX to work on experimental setup 929 - Gerardo moving pump cart from GV-5 to BSC1 for annulus pumping 945 - Kyle verifying picomotors off at EX, preparing to begin pumping 1004 - Kiwamu, Alexa doing projection work at HAM2 (WP 4782) 1008 - Fil and Manny working on cabling at EX 1129 - Bubba craning pelican case with test mass from West Bay to High Bay 1129 - Fred with small tour in LVEA 1202 - Projection work on IMC complete for now
Found cdswiki to be locked up and dead, console showed no display. Rebooted.
With the closing of most of the chambers recently, we are in a state where we can relieve Alarm Levels on some Dust Monitors (note: HAM6 is still open & we have exposed parts in the West Bay Test Stand area). At any rate, I went through Dust Monitors 1, 2, & 3 & raised their alarm levels (on the order of 10^2 counts for 0.3 & 0.5um). Could do this for other Dust Monitors which are away from clean hardware.
I notified Jeff Bartlett about this. Will chat with Calum about whether we want to establish long term values for these levels when we are all buttoned up.
Took a quick look at the FSS MEDM screen and noticed that the RFPD DC value was fluctuating wildly. Pulled up the filter for this channel and saw that the 2 Hz low-pass filter was not engaged and that the gain value was set to 1.000. The 2 Hz low pass filter is now engaged, as it should be, and the gain value was set to 0.150 which gives readings consistent with those obtained with a digital multimeter plugged into the DC output of the RFPD.
no restarts reported
Alexa, Dan, Koji, Sheila, Stefan, Kiwamu,
Today we spent some more time on alignment of the IMC with the use of the WFSs loops. After some struggling, we eventually could close all the loops stably. However, the ASC loops tend to drift on a time scale of 30 min.
In parallel to it, we made a first attempt of the ring down measurement. The data did not make sense this time. Ongoing.
IMC alignment:
Our original hope was that once the WFSs were centered, they should be able to servo the IMC to a good alignment. However, it turned out that stably engaging the ASC loops were very difficult for some reason. The first issue we noticed was that the MC2 trans QPD did not show a reasonable signal. It looked all noise and indeed changing the whitening settings did not change the shape of the noise. This indicated some issues in the analog circuits. Stefan and Sheila went to the rack and found that a number of cables were unplugged. Also, they found that the whitening electronics were turned off. So they plugged the cables back to the whitening box and powered up the whitening box. This recovered signals on the MC2 trans QPD. This then allowed us to close the 'DOF3' loop which is the centering servo for the MC2 QPD.
However, we were still having a difficulty in closing the rest of two loops in the IMC ASC. They use the signals derived from the WFSs. The symptom is that the error signal looked too big even though the loops are closed. It looked as if the loop is not suppressing the signals. Acutually, keep running the ASC loops made the power buildup and visibility worse on a time scale of 30 sec or so. We made sure that the dark offsets were successfully removed and centering on these WFSs were fine. But, no success.
After people left, I did some more investigation on the ASC loops. Since I did not like the beam shape in the reflection camera, I went to the table and checked out the beam. I found that there was a ghost beam not being dumped and going into the WFSs. I narrowed the aparture of the iris that was infront of the REFL RFPD such that it catches the ghost beam. Then I digitally removed the dark offset from all the WFS segments and tried closing the ASC loops again. The loops stayed stable for approximately 10 min. However then it started degrading. See the attached. I am not sure why, but I am worried about RFAM. I am leaving the ASC loops running for the night to see the long term stability.
Ring down measurements:
We also spent some time trying to measure the cavity decay time (storage time) in order to estimate losses in the cavity. We tried various ways of shutting the control or light off, but ended up with switching the polarity of the fast signal in the IMC board. This is the same technique as Livingston did recently (LLO 13748). We were expecting to see something like 17 usec 1/e decay time, but the measurement tended to give us about 35 usec which is twice bigger than the expectation. At this point, it is unclear why the decay time is such long. The attached is a picture of the raw data displaced on an oscilloscope. The PD is Thorlabs, PDA100A on the IOT2L table. The bandwidh is 2.4 MHz according to the data sheet which should be fast enough for this measurement.
It maybe independent, but we know that this transmitted light is largely clipped (seemingly more than 20% of its total intensity) somewhere in chamber before it comes out to the IOT2L table. So we are interested in repeating this measurement at a different port. Maybe at REFL or IOT2R. The measurement is therefore ongoing.
The attached is a trend from the last night.
You can see that the alignment degrades on a time scale of ~ 2 hours. Every time it hit the lower threshold of the ASC trigger, the alignment was forced to be back to the starting point due to the 'clear history' operation in the ASC loops.
G. Moreno, K. Ryan, J. Worden, R. Weiss A preliminary report of the procedure is given here, a more thorough report will be made once the post injection charge measurements have made. We introduced both positive and negative ions of N2 into the ETMY chamber. The input gas was boil off from liquid nitrogen which was additionally passed through a liquid nitrogen trap before entering the ionizer. The conditions in the ionizer: pressure on the needles 210 to 303 torr, pressure after the apertures was a maximum 45 torr when the chamber was at 42 torr. We stopped the process after the ionizer had become too cold to be comfortable with a elastomer O ring at the needles. (We should have a second heat exchanger to warm the gas back to room temperature before entering the ionizer to avoid the cooling.) The various times: start to stop of the ion injection 29 minutes, roughing pump down time after the injection to reach 1 torr about 3 hours, pressure now 3.5 x 10^-7 torr after 5 hours of turbo pumping. A disappointment of the procedure was that we were never able to achieve equal injection of positive and negative ions, the sampled ion current was: i+ = 4 x 10^-9 ampere, i- = -1 x 10^-9 amps. The injected currents are about 100 times larger. It requires tuning of the pressure on the needles and the flow rate to achieve equal positive and negative currents. If the total gas flow is too large one cannot get to the proper tuning. This was the case today. RW made a mistake in fully opening the gate valve between the chamber and the ionizer before tuning the system in an auxiliary flow to a pump and then gently transferring the flow between the pump and the chamber. There is a reasonable chance that enough ions did enter the chamber to neutralize the etmy. The success or failure should be known shortly after the morning meeting. If the neutralization has failed we could try again today. The times are shorter than estimated.
J. Kissel, K. Venkateswara After gathering a "first light" performance measurement of the H1 EX Beam Rotation Sensor (see first attachment -- the system is at air, poorly thermal shielded, and auto collimator is not well-secured to structure), we've spent nost of the day characterizing the separation between suspension point and center of mass, or "d". The goal is to have this separation be as small as possible, to maximize the rejection of translation noise. We're running one final 1 [mHz] data point over night to confirm, but we believe the C.o.M. is currently 20+/-4 [um] above the suspension point. We think we should be able to get this down to 2 [um], with an overall mass adjustment, which we'll do tomorrow. The second attachment shows the process -- drive the platform at X [mHz], measure the ASD, and since we do not change the amplitude of excitation, this is a direct map of the Beam Tilt / Ground Tilt transfer function. In reality, we make a fit to a sine wave to gather the amplitude with more precision and to have an uncertainty estimate. The first page shows a single measurement to demonstrate our signal is well above the noise floor, the second shows the collection of measurements in the form of an ASD, and the final page shows the modeled transfer function against our measurement points.
=== Rack ISC-R2 U38 ===
H1:ISC-RF_C_REFLAMP45M_OUTPUTMON = 17.5009
seems low by ~3dB. Corresponing demods seem low too.
Reflected to the original post. They should be checked next week.