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Reports until 16:05, Friday 21 January 2011
H2 General
dani.atkinson@LIGO.ORG - posted 16:05, Friday 21 January 2011 (500)
Ops Day Shift Summary
  • Stack was removed from BSC8 and dome placed back.
  • Oscar baled some tumbleweeds.
  • Ski and the squeezers craned an ISC table over the X-arm, to be placed in the East Bay laser hazard area.
X1 SUS
jeffrey.bartlett@LIGO.ORG - posted 16:39, Thursday 20 January 2011 (499)
Quad 2 Weights
Andres and I weighed the Q2 US and UI Masses.

    (1). Upper Structure - 254lbs  Note: The Cross Braces and their corresponding fasteners are not fit.
    (2). UI Test Chain - 21.526Kg
    (3). UI Reac Chain - 21.532Kg 
H2 INS
patrick.thomas@LIGO.ORG - posted 16:16, Thursday 20 January 2011 (498)
Ops Day Summary
Jake from SnoValley working on glycol pump
Dale took pictures in LVEA
Terry craned the auto scrubber over the beam tube
Terry, Christina, and Gerardo Jr. cleaned around BSC8
Kyle vented YBM
BSC8 door and dome were removed and covered
Dani put locks on H1 PSL enclosure
H2 DAQ
corey.gray@LIGO.ORG - posted 16:04, Thursday 20 January 2011 (497)
BSC8 Door & Dome Removed In Prep For Seismic Isolation De-Install

[Chris, Corey, Hugh, Jim, Kyle, Zach]

The BSC8 Door was removed.  Jim entered chamber and removed the (18) inside Support Tube bolts.  Dome was removed, and Chamber was covered.  De-install & re-install of Dome will occur tomorrow.

LHO FMCS
kyle.ryan@LIGO.ORG - posted 15:29, Thursday 20 January 2011 (496)
Vented YBM
Kyle - Valved-in aux. pump cart to GV5 annulus, vented YBM -> Leak from YBM to Vertex (known) -> Using aux. pump cart on GV1 annulus.  

Kyle, Chris, Zak, Rodney, Hugh, Corey - Removed BSC8 south door.
LHO FMCS
dani.atkinson@LIGO.ORG - posted 11:46, Thursday 20 January 2011 (495)
PSL Enclosure Locking
In preparation for the squeezers' reactivation of the PSL, the enclosure has been modified to allow it to be mechanically locked when the laser is running, reducing our reliance on the interlock system and adding a layer of safety in place of wearing glasses in the LVEA.

Pictured below, the inner doors are held in place by aluminum 3/4" x 3/4" bars only accessible by opening the front doors, while the front doors are prevented from moving by padlocks secured through holes drilled into the sliding tracks. The padlocks are all similarly keyed and the key will be kept in the control room.

Note that even with this system in place it's still possible to move some of the doors enough to trigger a violation.
Images attached to this report
LHO FMCS
kyle.ryan@LIGO.ORG - posted 19:50, Wednesday 19 January 2011 (494)
Corner Station purge air off from ~1100 -~1900


			
			
LHO FMCS
kyle.ryan@LIGO.ORG - posted 19:39, Wednesday 19 January 2011 (493)
YBM vent (preparation) and purge air oil!
Hard-closed GV5, soft-closed GV6, isolated IP5, connected aux. pump cart to GV5 annulus (did not valve-in), spun-up YBM MTP -> all in preparation of venting YBM -> Did not vent YBM as scheduled.  Had shut down purge air compressor in the morning to inspect internals of airbox and ended up spending the rest of the day disassembling the airbox, cleaning and caulking leaks noticed between the sheet metal stitch welds which were allowing compressor cabinet air to enter the compressor downstream of the inlet air filter.  The compressor crankcase vents inside of the cabinet and this air is laden with turbine oil vapor.  This air was entering the 1st stage compressor inlet by way of small unsealed passages (gaps) which occur between the welded sheet metal airbox stitch welds. Inlet air is intended to enter from LVEA ducting only.  Evidence of condensed oil was noticed in the intercooler condensate drain bowl but nowhere else downstream -> I showed John W. the details of my concern.  In addition to caulking, I fabricated gaskets for the bolted sheet metal components of the airbox.  These steps are expected to eliminate cabinet air from entering the compressor intake.
X1 SUS
travis.sadecki@LIGO.ORG - posted 16:12, Wednesday 19 January 2011 (492)
BS/FM (FM1) first full hang
Today I successfully fully hung the BS/FM (FM1) for the first time.  After several rebuilds of the wire loop/middle wire assembly due to kinks and breakage (2 more rebuilds today after Betsy's last post), a complete hang and rough adjustment was completed.  After setting the blade tip positions in the top mass, I released it and the top stage from their stops.  The initial pitch of the top mass was out ~10 degrees, during which time I noticed that due to the off-center position in which the wire exits through the base plate of the top mass (see pic 6), the wires were touching the edge of the base plate holes.  This is something to watch carefully for in subsequent assemblies as a more severe pitch issue could damage the wire assemblies enough to warrant a rebuild.  I would recommend slowly lowering the EQ stops until it becomes apparent that this is not an issue.  If it seems to be, stop and reclamp the mass until enough mass is shifted to hang level.  It did not seem that the contact was severe enough to gouge or bend the wires, so I proceeded to move addable masses around on the top mass, as it became apparent that that the pitch adjuster screw would not have enough range to remove all the mis-pitch.  In all, I had to move ~200 grams of masses to the OSEM side of the mass.  Having done that, all the DOFs look rather good.  However, the chain does appear to be hanging biased toward one side of the structure, so I will have a look at centering it up using the top stage adjustment tomorrow.  
Images attached to this report
H2 General
jeffrey.garcia@LIGO.ORG - posted 15:57, Wednesday 19 January 2011 (491)
Ops Day Summary
~9:45 – Kingsoft arrives on-site

~10:00 – Dani adding safety fixtures to PSL table

~10:30 – SnoValley arrives on-site

~10:45 – Kyle notifies Control Room he will shut down the purge air compressor in the Corner Station.  

~2:45 – Oscar and crew finished baling tumbleweeds

other activities throughout the day: 

Cleaning around BSC 8.  To be continued tomorrow.
H2 INS
patrick.thomas@LIGO.ORG - posted 13:20, Wednesday 19 January 2011 (490)
dust monitors moved
Dust monitor location 4 moved into the clean room around BSC8
Dust monitor location 8 temporarily removed, sensor fail.
H2 General
michael.rodruck@LIGO.ORG - posted 16:02, Tuesday 18 January 2011 (489)
Ops Day Summary
H2 INS
john.worden@LIGO.ORG - posted 15:04, Tuesday 18 January 2011 (488)
Recycled Metal
The first bin of aluminum(~5000lbs) from the iLIGO stacks was picked up this afternoon. An empty bin (for SS) was left on site ready for loading.
LHO FMCS
john.worden@LIGO.ORG - posted 15:00, Tuesday 18 January 2011 (487)
OSB Air Handler 3
I reduced the heater setting for AHU3 hot deck. One stage remains on.
H2 INS
corey.gray@LIGO.ORG - posted 14:05, Tuesday 18 January 2011 (486)
H2 BSC4 Scissors Tables Centered

BSC4's Scissors Tables were centered vertically, and Stop Links were installed on them to keep them centered.  Attached are photos showing 1) the Stop Link & the Slotted Link, and (2) a creepy spider-webbed Scissors table.

Images attached to this report
LHO FMCS
kyle.ryan@LIGO.ORG - posted 17:10, Friday 14 January 2011 (485)
XBM
Kyle, Chris, Zak -> Installed BSC7 east door

Kyle -> Pumped XBM down to ~32 torr. Will resume pumping on Monday.
H2 General
jeffrey.garcia@LIGO.ORG - posted 16:01, Friday 14 January 2011 (484)
Ops Day Summary
9:30 – work in LVEA to move HAM7,8,9 Optics Tables & BSC6,7 Downtubes/Optics Tables to the recycling bin

10:15 – Roger's Machinery to work on pumps with Kyle

10:30 – Dani in the LVEA modifying PSL table enclosure

12:00 – ISI passive stack removal work finished

1:30 - Kyle notified the Control Room he was to begin putting the door back on BSC7

12:15 – Michael R. making PSL measurements in LVEA

1:30 – Dani installing LED lights in outbuildings

X1 SUS
betsy.weaver@LIGO.ORG - posted 15:58, Friday 14 January 2011 (483)
FM1 build
Today, we loaded the weight adjusted (to 12,630g, nominal 12,621g) Top Mass into the Table cloth mounted in the structure.  Our first attempt at stringing the middle wires up from their attachment point on the Penultimate Mass to the Top Mass failed when we dropped one of the 4 top clamps causing a kink in the wire (recall these are long and unwieldy and get threaded through the structure, a very delicate 2 person task).  After disassembling the multi-segment set of wires again, we fixing the kinked one and re-threaded it.  We then leveled the Top Mass and hung the Pen and Test Mass.  We were in the middle of adjusting the 4 blade tip heights and lateral positions in the Top Mass when we accidentally broke a middle wire with a tool.  We have disassembled the wire segment again and fixed it, but stopped there for this week.  The learning curve continues on the BS type suspension triple.
Logbook Admin Bug
cheryl.vorvick@LIGO.ORG - posted 14:01, Friday 14 January 2011 - last comment - 17:09, Thursday 15 September 2011(482)
Quick Search issues
When hitting "enter" in quick search, it doesn't execute the search, it just returns the entire alog.
Comments related to this report
jonathan.hanks@LIGO.ORG - 17:09, Thursday 15 September 2011 (1412)
Fixed Sept 2011.
H2 General
cheryl.vorvick@LIGO.ORG - posted 13:50, Friday 14 January 2011 (481)
Removed Camera from HAM8 top viewport (H2PMX)
I've removed the H2 PMX camera that was on HAM8, and covered the viewport with a yellow blank.

H2PMX lighting (LED light) is still mounted to the HAM8 West wall on the most North viewport.  It can remain, or be removed at any time.
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